65 consumer complaints have been filed with NHTSA for the 1997 Hyundai Accent. Click any complaint to view the full owner description.
LATCHES/LOCKS/LINKAGESJune 13, 2011
TL* THE CONTACT OWNS A 1997 HYUNDAI ACCENT. THE CONTACT STATED THAT THE DOOR LATCHES ON ALL FOUR DOORS OF THE VEHICLE WERE DETACHING. THE DRIVER SIDE DOORS AND LATCHES WERE COMPLETELY INOPERABLE. THE CONTACT WOULD HAVE TO ENTER AND EXIT THE VEHICLE THROUGH THE PASSENGER DOOR. NEITHER THE DEALER NOR THE MANUFACTURER WAS CONTACTED. THE FAILURE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS 107,000 AND THE CURRENT MILEAGE WAS 120,000.
AIR BAGS,EQUIPMENTDecember 19, 2007
DEAR SIR I WOULD LIKE TO BRING THE SURPRISING ISSUE IN FRONT OF YOU RELATED TO HYUNDAI ACCENT I HAVE BEEN DRIVING FOR MORE THAN A YEAR NOW. I WAS DRIVING THIS CAR ON THE 401 EAST HIGHWAY, ONTARIO, CANADA ON 16TH DECEMBER 2007 AT 2.35 P.M. MY WIFE AND MY LITTLE ONE AND A HALF YEAR DAUGHTER WERE ALSO ACCOMPANYING ME. I WAS COMING FROM WINDSOR AND HEADING TOWARDS TORONTO. SUDDENLY THE AIR BAG OF THE DRIVER SEAT BLEW UP WITHOUT ANY COLLISION OF MY CAR WITH ANY THING. I WAS LUCKY ENOUGH THAT I WAS DRIVING IN THE RIGHT LANE AND MANAGED TO BRING MY CAR OUT OF THE DRIVING LANE. DUE TO ALMIGHTY'S GRACE NO CAR WAS FOLLOWING ME OTHERWISE THAT WOULD HAVE LEAD TO A DISASTER. I WAS AMAZED TO SEE THIS IN FRONT OF MY EYES THAT HOW COULD AIRBAG OF THE CAR BLEW UP WITHOUT ANY COLLISION. I AM CONFIDENT THAT THIS WOULD HAVE SURPRISED YOU TOO THAT HOW COULD YOU MANUFACTURE SUCH A DREADFUL VEHICLE IN WHICH THE PARTS ACTIVATE AT THE WRONG TIME AND COULD LEAD TO ACCIDENTS INSTEAD OF ACTIVATING FOR THE SAFETY OF PASSENGERS. I AM THANKFUL TO 911 EMERGENCY THAT THEY CAME ON TIME AND TOOK US OUT OF THE SITUATION AND WE MANAGED TO REACH BACK HOME SAFELY. I IMPRESS UPON YOU TO LOOK INTO THIS SERIOUS ISSUE AS SOON AS POSSIBLE. I AM ALSO INTERESTED TO BRING THIS ISSUE TO OTHER CAR MANUFACTURERS AND LEGAL DEPARTMENTS WHICH HAVE AUTHORIZED YOU TO MANUFACTURE CARS WITHOUT TAKING THESE THINGS INTO CONSIDERATION AND THE PASSENGERS HAVE TO PUT THERE LIVES ON RISK DUE TO YOUR SHEER NEGLIGENCE. I WOULD LIKE YOU TO COMPENSATE ME FOR ALL THE HASSLES AND RISK OF LIFE MY FAMILY AND I HAVE BEEN THROUGH AND PROVIDE ME WITH OTHER CAR WHICH IS FULLY CHECKED. I SPOKE WITH THE REPRESENTATIVE MS. MITCHEL AT THE HYUNDAI AMERICA NO. SHE HAS REGISTERED THIS SERIOUS ISSUE AND ASSIGNED CLAIM NO. 3182613. I WOULD LIKE THIS MAIL TO BE FORWARDED TO THE CONCERNED PERSON AS SOON AS POSSIBLE SO THAT THEY CAN LOOK INTO THIS MATTER SERIOUSLY. THANKS AND REGARDS RAJAN MALHOTRA *TR
FUEL SYSTEM, GASOLINEAugust 20, 2007
I HAVE AN APPOINTMENT THIS WEEK FOR WHICH THE DEALER WANTS TO CHARGE ME $99 TO INSPECT A CRACKED FUEL TANK PER RECALL IN WHICH POSSIBLY 66,086 VEHICLES OF MY TYPE ARE INVOLVED. I HAVE THE FEELING THAT THE DEALER WILL TRY NOT TO COVER THIS REPAIR. SEE MY DETAILS BELOW. RECALL CAMPAIGN: 00V314001. SHOULD THE DEALER BE RESPONSIBLE FOR THIS REPAIR? THIS CAR IS IN PERFECT SHAPE DESPITE THE MILEAGE. IT HAS NEVER BEEN HIT, TOWED OR IMPROPERLY JACKED. I HAVE A 1997 ACCENT GT ( MFG 04/16/97). I WAS NOTIFIED BY MAIL SOME MONTHS BACK THAT THE GAS CAP NEEDED TO BE REPLACED TO PREVENT EXCESS PRESSURE BUILDUP IN THE TANK THAT MIGHT LEAD TO THE TANK CRACKING. I WENT TO THE LOCAL DEALERSHIP, EARNHARDT HYUNDAI IN GILBERT, AZ, AND THEY REPLACED THE CAP AS SPECIFIED AND SUPPOSEDLY PRESSURE TESTED THE TANK. NOT LONG AFTER THAT I BEGAN TO SMELL FUMES WHENEVER I FILLED UP AND THE SMELL CONTINUED FOR 50 TO 75 MILES BEFORE ABATING. I DROPPED THE TANK AND CHECKED EVERYTHING I COULD FIND, REINSTALLED, AND STILL HAD THE PROBLEM. TODAY I DROPPED THE TANK AGAIN AND UPON CLOSE INSPECTION I FOUND A SMALL CRACK (ABOUT 1/2 INCH) IN THE MIDDLE OF THE TOP OF THE TANK. CLEARLY THE TANK NEEDS TO BE REPLACED BUT "IS THERE IS AN IMPROVED TANK?" AND "WILL IT BE COVERED IN CONNECTION WITH THE GAS CAP RECALL?" SINCE CAUSE AND EFFECT HAS BEEN DEMONSTRATED. THE DEALERSHIP IS NOT COOPERATING WITH THIS REPAIR. IT IS MY COMPLAINT AND DEMAND THAT HYUNDAI MUST PROVIDE FULL, PROMPT REMEDY FOR THIS POTENTIALLY DANGEROUS (FLAMMABLE) DEFECT BUT HASN'T DONE SO. THIS CAR HAS 162,640 MILES (BUT RUNS LIKE NEW!). DON'T GET THIS WRONG, IT IS A GREAT CAR BUT HAS A SERIOUS DEFECT AND HYUNDAI IS NOT STEPPING UP TO TAKE RESPONSIBILITY FOR THE REPAIR WHICH THE DEALER ESTIMATES WILL COST APPROXIMATELY $350 TO FIX. OPTIONAL INFORMATION: 1997 HYUNDAI ACCENT 1.5L DOHC. *TR
SUSPENSION,SERVICE BRAKES, HYDRAULICAugust 13, 2007
RIGHT FRONT COIL SPRING BROKE HITTING ROTOR CRACKING THE ROTOR REPLACED ALL AFFECTED PARTS AT OUR OWN EXPENSE REPLACED COIL SPRING,ROTOR,BRAKE PADS. HYUNDAI SAYS THIS VEHICLE NOT IN THE RECALL EVEN THOUGH IT IS REGISTERED IN THE EFFECTED AREA OF THE RECALL THIS COULD HAVE POTENTIALLY LED TO CATASTROPHIC FAILURE IF IT HAD NOT BEEN DETECTED. *TR
LATCHES/LOCKS/LINKAGESAugust 3, 2005
THE DRIVER SIDE DOOR LATCH ON MY '97 HYUNDAI SONATA BROKE AND ITS REALLY BIG SAFETY CONCERN. I'VE BEEN LOOKING ON THE INTERNET AND ITS NOT JUST ME WHO HAS THAT PROBLEM THE DOOR LATCH BREAKS EASILY AND IT COSTS A LOT OF MONEY TO GET IT FIXED SINCE THE PART COSTS $93 +. AND SINCE THE DOOR CAN'T OPEN ITS GOING TO COST A LOST OF MONEY FOR LABOR BECAUSE THEY HAVE TO GET THE DOOR OPENED SOMEHOW AND LABOR GOING TO BE VERY EXPENSIVE. HERE'S THE WEBSITE THAT REFERRED ME: HTTP://WWW.CARSURVEY.ORG/VIEWCOMMENTS_REVIEW_46625.HTML. *NM
FUEL SYSTEM, GASOLINEDecember 7, 2004
THE SMELL OF FUEL PROMPTED THE CONSUMER TO MAKE CONTACT WITH THE MANUFACTURER AND THE DEALER SINCE THERE WAS A FUEL TANK RECALL. CONSUMER LOCATED A CRACK ON THE FUEL TANK. THIS VEHICLE WAS NOT INCLUDED IN THE NHTSA RECALL 00V314000. *AK
STEERING,AIR BAGSNovember 30, 2004
WHILE DRIVING CONSUMER HAD AN ACCIDENT. UPON IMPACT, AIR BAGS DID NOT DEPLOY. CONSUMER WAS INJURED. ALSO, CONSUMER STATED THAT THE GUIDING ARM WAS VERY WEAK. THIS CAUSED PROBLEMS WITH THE STEERING.*AK
Crash reported1 injury(ies)
NHTSA #10101835SERVICE BRAKES, HYDRAULICNovember 19, 2003
CONSUMER STATED WITHOUT ANY INDICATION REAR BRAKES LOCKED UP.*AK
AIR BAGSSeptember 2, 2003
THE AIR BAG WARNING LIGHT STAYED ON CONTINUOUSLY. THE CONSUMER IS CONCERNED THAT THIS MAY CAUSE PREMATURE DEPLOYMENT OR NONE DEPLOYMENT OF THE AIR BAG. THE DEALERSHIP HAS BEEN NOTIFIED.*AK *NLM
POWER TRAINApril 3, 2003
CAR WAS RETURNED TO HYUNDAI UNDER WARRANTY IN JANUARY 2002. REPORTED TO HAVE A BAD TORQUE CONVERTER AND STARTER. BOTH REPLACED UNDER WARRANTY. LAST WEEK CAR WOULDNT START AGAIN. OUR MECHANIC DIAGNOSED SAME PROBLEM. WAS TOLD THAT IF CAR HAD BEEN PROPERLY DIAGNOSED AS HAVING EXTENSIVE TRANSMISSION PROBLEM WHILE UNDER WARRANTY THIS WOULD HAVE BEEN PROPERLY REPAIRED AND NOT PATCHED UP. HYUNDAI IS NOW REFUSING TO ABSORB COST SINCE THE CAR IS NO LONGER UNDER WARRANTY. TORQUE CONVERTERS AND STARTERS DONT GO BAD YEARLY!!! HELP!!
POWER TRAINSeptember 24, 2002
CONSUMER STATES THAT WHILE DRIVING AT ANY SPEED AND NO WARNING THE VEHICLE WILL HEAVILY JERK AND THEN THE ENGINE LIGHT WILL COME ON AND WILL STAY ON THE REMAINDER OF THE TIME VEHICLE IS BEING OPERATED. DEALER NOTIFIED. NLM
SUSPENSIONJune 24, 2002
THE PARTS THAT BROKE WERE ON THE SWAY BAR WHERE IT ATTACHES TO THE CONTROL ARM. *AK
AIR BAGSMarch 6, 2002
WHILE STOPPING, WAS REARENDED BY ANOTHER VEHICLE AND PUSHED FORWARD, AIR BAGS DID NOT DEPLOY. DRIVER INJURED AND VEHICLE WAS TOTALED.*AK CONSUMER STATES THAT THE FRONT END OF THE VEHICLE WAS COMPLETELY SMASHED. *SLC
Crash reported1 injury(ies)
NHTSA #8005082ENGINE AND ENGINE COOLINGFebruary 1, 2002
VEHICLE STALLS WITHOUT PRIOR WARNING. DEALERSHIP IS AWARE OF PROBLEM.*AK
ENGINE AND ENGINE COOLINGNovember 30, 2001
WHILE DRIVING 55MPH THE VEHICLE STALLED OUT AND DIED WITHOUT WARNING. DEALER HAS BEEN NOTIFIED. PLEASE PROVIDE ADDITIONAL INFORMATION.*AK
SUSPENSIONSeptember 11, 2001
FRONT COIL SPRING HAS DEVELOPED CRACKS. A RECALL HAS BEEN ISSUED ON VEHICLE'S MAKE/MODEL. HOWEVER, THIS VEHICLE WAS NOT INCLUDED DUE TO VIN. VEHICLE HAS BEEN REPAIRED AT OWNER'S EXPENSE. PLEASE PROVIDE FURTHER INFORMAITON.*AK
ENGINE AND ENGINE COOLINGJuly 8, 2001
NO SUMMARY LISTED FOR ABOV EVEHICLE. *AK
ELECTRICAL SYSTEMJune 21, 2001
ENGINE WILL TURN OVER BUT NOT START THIS HAPPENS SEV TIMES. *AK
VISIBILITYMay 3, 2001
WE WERE LEAVING FOR VACATION IN NEW JERSEY, DRIVING WESTBOUND ON I-26, AT THE POSTED SPEED LIMIT, JUST EAST OF THE ST. GEORGE EXIT. WHEN THE SOUND OF AIR RUSHING INTO THE CAR BECAME APPARENT. THE SUN ROOF PREVIOUSLY UNOPENED THAT DAY, STARTED SHAKING, AND FLIPPED BACKWARDS DENTING THE ROOF. THE REAR CATCH BROKE OFF AND THE ENTIRE ASSEMBLY THEN FLEW OFF INTO TRAFFIC. THE VEHICLE WHICH NARROWLY AVOIDED THE ROOF ASSEMBLY PULLED OVER TO THE SIDE AS DID WE. THEY TOLD US THEY WERE ALRIGHT AND WE ALL THANKED GOD THEN THEY WERE ON THEIR WAY. IT WAS RATHER LATE IN THE EVENING BUT WE DECIDED TO GO TO THE DEALER ANYWAY. THE GENERAL MANAGER TOLD US THERE WAS NOTHING HE COULD DO AND TO COME BACK WHEN SERVICE WAS OPEN, THE NEXT MORNING. WE THEN WENT HOME AND CALLED LOCAL POLICE. THEY CALLED THE STATE POLICE, WHO INFORMED US THAT IT WAS A "FREAK-ACCIDENT" AND TO TALK TO THE DEALER AND OUR INSURANCE COMPANY. ON SATURDAY WE WENT TO THE DEALER AND THE ASSISTANT SERVICE MANAGER, JASON, TOLD US THERE WAS NOTHING HE COULD DO UNTIL MONDAY, WHEN THEY WOULD CHECK FOR A DEFECT. IN THE MEANTIME, HE OBTAINED A RENTAL CAR FROM ENTERPRISE TO CONTINUE OUR TRIP, AND FILED THE CLAIM AS A WARRANTY PROBLEM. UPON TAKING THE CAR HOME WE FOUND THAT THE RENTAL CAR WAS UNSAFE TO DRIVE DUE TO INOPERABLE SIDE MIRRORS, SO WE TOOK OUR OTHER CAR. WE CALLED FROM NEW JERSEY ON MONDAY, BUT JASON WAS NOT IN AND NO ONE ELSE KNEW ANYTHING ABOUT THE SITUATION AND THEY SAID THEY WOULD HAVE HIM CALL. JASON CALLED THURSDAY TO INFORM US THAT THERE IS NO DEFECT AND THE PROBLEM IS NOT WARRANTEED. HE ALSO SAID THAT WE MUST RETURN THE RENTAL CAR BECAUSE THE COST WOULD NOT BE COVERED BY THE DEALER SINCE IT IS NEITHER A DEFECT NOR UNDER WARRANTY. JASON TOLD US TO REPLACE THE MOON ROOF THE JOB WOULD COST APPROX. $1500+, NOT INCLUDING SUBSEQUENT DAMAGE TO THE VEHICLE. WE THEN CALLED HYUNDAI MOTOR AMERICA CUSTOMER SERVICE, THE REP. TOLD US THAT IT COULD BE COVERED AS GOOD-WILL, WITH RENTAL ASSIST.
ENGINE AND ENGINE COOLING,POWER TRAINMay 3, 2001
FOR THE PC SYSTEM PROBLEM, I HAD NOTICED THAT THE PC VALVE WAS LEAKING OIL AROUND IT, SO I REPLACED THE COMPONENT ON MAY 12,2000. BY DECEMBER, I NOTICED THAT THE CAR HAD SOME SORT OF PROBLEM WITH A NOTED DROP IN PERFORMANCE AND FUEL ECONOMY. SO I DECIDED, BEFORE BRINGING THE CAR IN FOR MAINTENANCE, TO VISUALLY CHECK THE FLUIDS, AND WEAR COMPONENTS. I ENDED UP FINDING SLUDGE IN THE ENGINE, CREATED BY WATER IN THE OIL. WHEN DODGE/HYUNDAI OF PARAMUS CHECKED-OUT THE CAR THEY TOLD ME THE PROBLEM WAS A CLOGGED PC SYSTEM AND IT WAS NOT COVERED BY ANY WARRANY, SO I PAID FOR THE WORK. FOR THE TRANSMISSION PROBLEM I NOTICED THAT IT WAS LEAKING, AND WHEN THE DEALER IN PARAMUS CHECKED-OUT THE PROBLEM, THEY TOLD ME THAT SOMEONE HAD OVER-TORQUED THE OIL PAN, BLOWING OUT THE GASKET. THEY TOLD ME THAT THE PROBLEM SHOULD BE WARRANTEED BY ALTMAN IN N.CHARLESTON, SINCE THEY DID THE 30K CHECK-UP. WHEN I INFORMED ALTMAN, THEY TOLD ME THAT PARAMUS SHOULD HAVE DONE THE WORK AS WARRANTEED. SO, MIKE AT ALTMAN TOLD ME I WOULD RECEIVE A REFUND, BUT I NEVER DID, AND MIKE DOEN'T WORK THERE ANYMORE, AND NO ONE ELSE KNOWS ANYTHING. I TALKED TO HYUN. MOTOR AMER. CUST. SERVICE, AND I AM CURRENTLY WAITING FOR A CALL BACK. WHAT I WANT TO KNOW IS IF EITHER OF THESE IS COVERED BY WARRANTY, AND IF SO WHAT THEN?
ENGINE AND ENGINE COOLINGMarch 29, 2001
WATER PUMP AND HEAD GASKET BLEWOUT. DEALERSHIP WAS AWARE OF PROBLEM.*AK
POWER TRAINMarch 28, 2001
TRANSMISSION FAILED AND HAD TO BE REPLACED. PLEASE PROVIDE ANY ADDITIONAL INFORMATION/ATTACHMENTS.*AK
FUEL SYSTEM, GASOLINE,UNKNOWN OR OTHERMarch 28, 2001
ENGINE CHECK LIGHT COMES ON AND OFF WHILE CONSUMER HAS OWNED VEHICLE. THIS OCCURS MORE FREQUENTLY WHEN GAS TANK IS FILLED TO HALFWAY MARK. DEALERSHIP HAS REPLACED SEVERAL COMPONENTS OF VEHICLE, AND STILL HAS NOT RESOLVED PROBLEM. PLEASE PROVIDE ANY ADDITIONAL INFORMATION/ATTACHMENTS.*AK
FUEL SYSTEM, GASOLINE,UNKNOWN OR OTHERFebruary 9, 2001
CONSUMER WAS TRAVELING ON A CITY STREET AND ENGINE CHECK LIGHT CAME ON DASHBOAD. ALSO, THERE WAS A GASOLINE SMELL AND VEHICLE CAUGHT ON FIRE. *AK
Fire reported
NHTSA #880280ELECTRICAL SYSTEMFebruary 2, 2001
WHEN TRYING TO START VEHICLE SOMETIMES IT MAKES A LOUD GRINDING NOISE OR IT WILL NOT START AT ALL. CONSUMER HAS HAD 2 STARTERS PUT IN. FIRST ONE WAS WITH IN FIRST SIX MONTHS OF OWNING CAR. *AK
POWER TRAINJanuary 30, 2001
CAR STALLS, RUNS ROUGH WHEN COMING TO A STOP. I BOUGHT IT FROM THE DEALER ON 9/17/99 FOR $8,068.96 INCLUDING FINANCE CHARGES. IT HAD 45,490 MILES. NOW IT HAS 68,841 MILES. THE DEALER SAID IT WOULD COST $1,600 TO REPAIR THE TRANSMISSION PROBLEM. WHEN I ASKED ABOUT TRADING IT IN, THEY TOLD ME THE VALUE OF THE CAR IS ONLY $2,000. HOW DID IT DEPRECIATE SO MUCH IN ONE YEAR? IS THERE A RECALL ON THIS CAR? IS THE DEALER REQUIRED TO REPAIR THE TRANSMISSION UP TO 100,000 MILES REGARDLESS OF WHETHER I BOUGHT THE EXTENDED WARRANTY?*AK
ENGINE AND ENGINE COOLING,AIR BAGSSeptember 21, 2000
ON OR ABOUT MARCH 4, 2000, THE SUBJECT VEHICLE WAS INVOLVED IN AN AUTO ACCIDENT, AT WHICH TIME THE DRIVER REAR ENDED ANOTHER VEHICLE DRIVING AT APPROXIMATELY 30-35 MPH. BOTH THE PASSENGER SIDE AND DRIVER SIDE AIRBAGS FAILED TO DEPLOY. SOON THEREAFTER, THE ENGINE LIGHT BECAME ILLUMINATED. AFTER TAKING TO FARRISH IN MANASSAS, VIRGINIA, IT WAS REPORTED THAT THE COMPUTER INDICATED THAT I THE ENGINE WAS OUT OF TIME. THE TIMING BELT WAS REPLACED AND DID NOT CURE THE PROBLEM. I WAS THEN TOLD I NEEDED A TUNE-UP, WHICH WAS SUBSTANTIALLY DONE AND DID NOT CURE THE PROBLEM, WHICH LEADS TO MY BELIEF THAT THERE IS A MAJOR PROBLEM WITH THE EMISSIONS CONTROL SYSTEM. THE CAR NOW HEATS AND GETS HOT TO THE TOUCH AT THE FLOOR BOARD. THE MANUFACTURER HAS BEEN CONTACTED AND HAS FAILED TO INSPECT THE VEHICLE. I PLAN TOMORROW TO REVOKE MY ACCEPTANCE OF THE VEHICLE.
Crash reported
NHTSA #732192AIR BAGSAugust 25, 2000
VEHICLE WAS INVOLVED IN MOTOR VEHICLE ACCIDENT. DRIVER'S SIDE IMPACT. PASSENGER SIDE AIR BAG DEPLOYED FIRST. DRIVER, MY DAUGHTER STRUCK THE STEERING WHEEL AND THE DRIVER'S SIDE AIR BAG THEN DEPLOYED BURNING BOTH ARMS OF MY DAUGHTER. NO FRONTAL CONTACT AT ALL.
Crash reported1 injury(ies)
NHTSA #729118ENGINE AND ENGINE COOLING,VISIBILITYJuly 5, 2000
ENGINE IS DEFECTIVE AND HAS BEEN REPLACED ON 3 DIFFERENT OCCASSIONS UNDER WARRANTY. ALSO, ALL FOUR WINDOWS HAVE FALLEN ONTO THE DOORS. WINDOWS HAVE BEEN REPAIRED ON 4 DIFFERENT OCCASIONS. *AK
SERVICE BRAKES, HYDRAULICJune 20, 2000
CONSUMER WAS TRAVELING ABOUT 35MPH APPLIED BRAKES, AND THEY FELT VERY MUSHY. CONSUMER'S HUSBAND TOOK OVER & DROVE VEHICLE HOME, AND BRAKE PEDAL WAS GOING ALL THE WAY TO THE FLOOR. DEALER WAS CONTACTED & BRAKES WERE REPAIRED. THE CYLINDERS ON BOTH FRONT AND REAR BRAKES WERE LEAKING. THE CYLINDERS WERE CHANGED. MECHANIC SAID THE PARTS WERE DEFECTIVE. *AK *ML
AIR BAGSMay 9, 2000
CONSUMER'S VEHICLE REAR ENDED ANOTHER VEHICLE AT 20 MPH, AND THE AIR BAGS DID NOT DEPLOY. DEALER HAS NOT BEEN CONTACTED. *AK
Crash reported
NHTSA #861632ENGINE AND ENGINE COOLING,UNKNOWN OR OTHERApril 7, 2000
CAR LOT HAS ALREADY REPLACED O2 SENSOR TWICE, ENGINE CHECK LIGHT STILL COMES ON. *AK
POWER TRAINFebruary 7, 2000
TRANSMISSION GEAR GETS STUCK IN PARK AND BECOMES DIFFICULT TO SHIFT INTO DRVE. DEALER HAS BEEN CONTACTED, AND TOLD CONSUMER THAT THEY COULD NOT DUPLICATE THE PROBLEM. *AK
STRUCTURENovember 22, 1999
THE TWO LONG ARMS ON EACH SIDE OF THE HATCHBACK WINDOWS, LIKE TWO STRUTS, HAVE A BLACK OILY SUBSTANCE COMING OUT OF THE TWO POLES. CONSUMER HAS TO PROP HATCH BACK UP WITH A STICK, CONSUMER FEELS THAT IF DOOR FALLS ON SOMEONE'S HEAD IT COULD CAUSE SERIOUS HARM. DEALER SAID THEY COULDN'T FIX IT. TOLD CONSUMER THAT THEY COULD FIX IT. *AK
ENGINE AND ENGINE COOLING,ELECTRICAL SYSTEMSeptember 30, 1999
WHEN TURNING THE KEY IN THE IGNITION ENGINE DOES NOT TURN OVER. DEALER HAS REPLACED STARTER/ COMPUTER AN D CRANKSHAFT, BUT PROBLEM STILL EXISTS. *AK
ELECTRICAL SYSTEMJuly 27, 1999
WE BOUGHT THE VEHICLE IN NOV 1997. THERE WAS A HESITATION PRETTY MUCH FROM THE START...REALLY APPARENT AT 7581. WE BOUGHT IT BACK TO THE DEALER IN MARCH 1998...THEY ATTEMPTED TO REPAIR IT. IT CONTINUED TO BE A NUISANCE...WE CONTACTED THE DEALER AGAIN. WE BROUGHT THE VEHICLE IN TO BE REPAIRED ON JUNE 23, 1999. SINCE THEN THE SPARK PLUGS HAVE FAILED 4 TIMES (EACH TIME FAILURE WAS ON PLUG #1 AND #3). IT IS NOW JULY 27, 1999. THE IGNITION WIRES WERE REPLACED JULY 02... ONE OF THE WIRES REPLACED ON JULY 02 WAS REPLACED AGAIN JULY 07. WE HAVE REPLACED THE FUEL FILTER, HAD A THROTTLE BODY SERVICE AND A FUEL INJECTION SERVICE ...ALL TO NO AVAIL....THE PROBLEM IS WORSE THAN EVER. THE HESITATION OCCURS MOST OFTEN WHEN THE WEATHER IS AT HIGH TEMPERATURES , BUT CAN ALSO HAPPEN AT OTHER TIMES. I NOTICED THE ELANTRA DOHC ENGINE HAD ELECTRICAL SYSTEM WIRING...DOHC SPARK PLUG WIRE ROUTING PROBLEMS FOR A NUMBER OF YEARS. I WONDER IF THAT'S OUR PROBLEM ...OUR ACCENT GT IS ALSO A DOHC ENGINE !
SUSPENSIONJuly 14, 1999
STRUTS FAILED. MJS
SERVICE BRAKES, HYDRAULICJuly 14, 1999
ROTORS HAD TO BE WORKED ON ON TWO OCCASIONS. MJS
EQUIPMENTJuly 14, 1999
RADIO FAILED. MJS
ENGINE AND ENGINE COOLING,POWER TRAIN,SEAT BELTSJuly 6, 1999
AUTOMATIC FRONT SEAT BELTS WOULD NOT RELEASE AFTER BEING LOCKED. ALSO, CLUTCH FELL OUT WHILE DRIVING 55 MPH. VEHICLE LOST CONTROL. ENGINE LIFTERS ALSO WENT OUT. *AK
ENGINE AND ENGINE COOLINGJune 30, 1999
VEHICLE HESITATES WHILE DRIVING AT A STEADY SPEED, DEALER HAS REPLACED VACUUM LINES, COIL PACK, HOSES, CRANK SENSOR BUT PROBLEM STILL EXIST, DIAGNOSTIC TEST SHOWED NO ABNORMALITIES. *ET
ENGINE AND ENGINE COOLINGJune 30, 1999
VEHICLE HESITATES WHILE DRIVING AT A STEADY SPEED, DEALER HAS REPLACED VACUUM LINES, COIL PACK, HOSES, CRANK SENSOR BUT PROBLEM STILL EXIST, DIAGNOSTIC TEST SHOWED NO ABNORMALITIES. *ET
POWER TRAINMay 10, 1999
GREASE FROM FITTINGS FOR MASTER CYLINDER FOR CLUTCH GETS IN FLUID CAUSING THE INABILITY TO SHIFT GEARS. MJS
POWER TRAINMay 10, 1999
MANUAL TRANSMISSION REPLACED CAUSING GRINDING AND DIFFICULTY IN GOING INTO REVERSE. MJS
ELECTRICAL SYSTEMMay 10, 1999
IGNITION SWITCH/STEERING WHEEL LOCKS UP CONTINUALLY. MJS
AIR BAGSMarch 3, 1999
THIS IS A REQUEST FOR ADDITIONAL INFORMATION ON A AIRBAG ON/OFF SWITCH
AIR BAGSMarch 3, 1999
THIS IS A REQUEST FOR ADDITIONAL INFO FOR ON/OFF SWITCH FOR AIRBAGS
STEERING,SUSPENSIONFebruary 10, 1999
I JUST WANTED TO ADD THAT THE PROBLEMS WITH THIS CAR WHILE NOT FATAL AT THE PRESENT TIME COULD POSSIBLY RESULT IN SOMETHING FATAL IN THE VERY NEAR FUTURE. THE CAR WAS RETURNED TO THE NEAREST HYUNDAI DEALERSHIP, AND I WAS TOLD THAT IT WAS PRETTY MUCH MY PROBLEM. THE CAR IS VERY WELL MAINTAINED AND TAKEN CARE OF. THIS SHOULD NOT BE HAPPENING TO A CAR WITH LESS THAT 37000 MILES ON IT. I FEEL VERY UNSAFE DRIVING THE CAR, BUT I DO NOT HAE THE MONEY TO FIX IT. THAT IS THE REASON WHY I BOUGHT A BRAND NEW CAR. IF SOMEONE COULD HELP ME ON THIS IT WOULD BE GREAT. *AK
POWER TRAINFebruary 1, 1999
SHIFT LEVER FAILED CAUSING GEAR TO STICK WHEN PUT INTO DRIVE. *TT
AIR BAGSJanuary 26, 1999
CONSUMER HAD A FRONT END COLLISON AND AIR BAGS DID NOT DEPLOY, BOTH DRIVER AND PASSENGER WERE SLIGHTLY INJURIED.
Crash reported2 injury(ies)
NHTSA #833995SUSPENSIONDecember 30, 1998
DEALER IS NOT HONORING MFR. RECALL NOTICE REGARDING CORROSION OF FRONT COIL SPRINGS. *AK
ENGINE AND ENGINE COOLINGDecember 23, 1998
WHEN PUTTING GAS INTO THE TANK THERE IS A GRIDING SOUND COMING FROM THE VEHICLE, AND THE ONLY THING THAT IS MOVING IS THE GAUGE. VEHICLE ISN'T MOVING. VEHICLE WILL KICK IN AND THEN TAKE OFF. SOMETIMES WHEN THE CONSUMER IS COMING TO A STOP SIGN, HE WILL PUT THE VEHICLE INTO PARK JUST SO THE VEHICLE WON'T CUT OFF. THE VEHICLE SHAKES AND VIBRATES. VEHICLE HAS BEEN IN THE SHOP ABOUT SIX TIMES OR MORE, AND THEY CAN'T DETERMINE THE PROBLEM. *AK
ENGINE AND ENGINE COOLING,POWER TRAIN,TIRES,INTERIOR LIGHTINGDecember 8, 1998
BESIDES THE CLUTCH I HAVE HAD PROBLEMS WITH THE TIRES, SUN VISOR,THE TRUNK LIGHT AND WITH THE CAR STARTING. *MJS
POWER TRAINDecember 7, 1998
NO SUMMARY PROVIDED BY CONSUMER
VEHICLE SPEED CONTROLNovember 23, 1998
VEHICLE TOOK OFF BACKWARDS WHEN IGNITION SWITCH WAS TURNED ON, AND HIT ANOTHER CAR. INCIDENT OCCURRED AGAIN, AND DEALER IS AWARE OF THE PROBLEM. REPAIR WORK WAS DONE. *AK
Crash reported
NHTSA #831201AIR BAGSNovember 6, 1998
CONSUMER'S SON WAS DRIVING APPROXIMATELY 35MPH WHEN HE REAR ENDED A PONTIAC. THE DRIVER'S SIDE AIR BAG SLOWLY INFLATED. THE BLOCK DID NOT MOVE PROPERLY, IT WAS STUCK ON THE LEFT SIDE, ALLOWING THE AIR BAG TO INFLATE TO THE RIGHT SIDE OF THE DRIVER. THE DRIVER WAS THROWN INTO THE WINDSHIELD, THE PASSENGER SIDE BAG DID DEPLOY PROPERLY. ALSO, DRIVER SIDE SEAT BELT DID NOT LOCK UPON IMPACT. VEHICLE WAS TOTALLED. *AK
Crash reported1 injury(ies)
NHTSA #830333POWER TRAINSeptember 2, 1998
CLUTCH NOT ENGAGED ALTHOUGH CLUTCH PEDAL WAS DEPRESSED, CAUSING VEHICLE TO LURCH FORWARD WHEN IGNITION IS SWITCHED ON.
AIR BAGSAugust 19, 1998
OWNER DENIED AN AIRBAG CUTOFF SWITCH BY MANUFACTURER. REQUEST WAS MADE TO ALLOW A TODDLER TO RIDE IN THE FRONT PASSENGER SEAT.
ENGINE AND ENGINE COOLINGJuly 27, 1998
WHEN VEHICLE IS STOPPED OR SLOWS DOWN IT STALLS. DEALER HAS REPAIRED VEHICLE 4 TIMES. *AK
SUSPENSIONJune 22, 1998
ALL OF THE STRUTS HAVE GONE BAD ON VEHICLE . THE DEALER HAS BEEN NOTIFIED. *AK
ENGINE AND ENGINE COOLINGJune 13, 1998
CONSUMER COMPLAINTING OF VEHICLE KEEP CUTTING OFF AND STALLING WHILE DRIVING, THREE TIME VEHICLE BEEN IN/OUT OF DEALER SHOP FOR REPAIRS; CONDITION STILL OCCUR.
POWER TRAINFebruary 9, 1998
CONTAMINATED CLUTCH FLUID. BLED CLUTCH AND RESTORED CLUTCH PRESSURE.
ELECTRICAL SYSTEMJanuary 13, 1998
ELECTRICAL SYSTEM (SOLENOID WIRE FELL OFF).
ELECTRICAL SYSTEMJanuary 13, 1998
ALTERNATOR FAILED, CAUSING VEHICLE FIRE.
Fire reported
NHTSA #527952POWER TRAINOctober 27, 1997
CONSUMER STATES THAT WHILE DRIVING ABOUT 65 MPH , DOWNSHIFTING THE VEHICLE, THE GEARS STOPPED WORKING AND THE BRAKES WENT ON THE VEHICLE. THE DEALER HAS BEEN CONTACTED. *AK