Random Acceleration (Gas Pedal) when started from a cold start. When foot was not on any brake or gas pedal, van started to accelerate as if I had my foot on the gas pedal.
215 consumer complaints have been filed with NHTSA for the 1993 Ford Econoline. Click any complaint to view the full owner description.
Random Acceleration (Gas Pedal) when started from a cold start. When foot was not on any brake or gas pedal, van started to accelerate as if I had my foot on the gas pedal.
The contact owns a 1993 Ford E-150. The contact stated that upon attempting to pull into a parking space and turning the steering wheel, she heard an abnormal sound coming from underneath the front driver's side seat and the steering wheel seized. There was no warning light illuminated. The contact contacted AAA who inspected the vehicle and informed the contact that the gear box had detached from the subframe. The vehicle was towed to an independent mechanic where it was diagnosed that the front driver's side subframe had three holes and one of the holes had expanded significantly and needed to be welded prior to fastening the gear box to the subframe. The independent mechanic informed the contact that they could not weld the subframe. The dealer was notified and informed the contact that the next availability was in approximately two months. The vehicle was not repaired. The manufacturer was notified of the failure but provided no assistance. The failure mileage was approximately 200,000.
TL* THE CONTACT OWNS A 1993 FORD E-150. WHILE FUELING THE VEHICLE AT A FUEL STATION, THE FUEL WOULD LEAK OUT FROM THE TOP OF THE FUEL TANK. THE VEHICLE WAS TOWED TO THE CONTACT'S RESIDENCE. THE CONTACT WAS CONCERNED FOR HER SAFETY AND CALLED FIRMIN FORD (LOCATED AT 921 E MAIN ST, LAURENS, SC 29360, (864) 682-3111) TO SCHEDULE A DIAGNOSTIC APPOINTMENT. THE CONTACT WAS INFORMED THAT THERE WAS NO RECALL ON THE VEHICLE. THE VEHICLE WAS NOT TAKEN TO A DEALER AND WAS NOT REPAIRED. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE FAILURE MILEAGE WAS 186,000.
TL* THE CONTACT OWNS A 1993 FORD E-350 EQUIPPED WITH GOODRICH COMMERCIAL T/A (NA) TIRES, SIZE: LT225/75/R16E (NA). WHILE DRIVING 55 MPH, THE TREAD FROM THE REAR DRIVER SIDE TIRES SUDDENLY RIPPED OPEN AND DAMAGED THE BODY AND THE SEWAGE SYSTEM OF THE MOTOR HOME. THE MOTOR HOME WAS TAKEN TO A DEALER FOR DIAGNOSTIC TESTING WHERE IT WAS CONFIRMED THAT THE TREAD SEPARATED FROM THE REAR DRIVER SIDE TIRE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE APPROXIMATE VEHICLE FAILURE MILEAGE WAS 189,987 AND THE TIRE FAILURE MILEAGE WAS 40,980.
I WAS DRIVING ON I-95 WHEN MY VEHICLE STARTED THUMPING AND VIBRATING ERRATICALLY AND STEERING WAS VERY HARD TO CONTROL. I EXITED IMMEDIATELY TO FIND THAT MY TIRE HAD A HUGE BULGE A LITTLE LARGER THAN A SOFTBALL. A MAN STOPPED AND SAID I SHOULD BE OKAY TO DRIVE THE 2 MILES I HAD LEFT TO GET HOME. WHEN I BACKED OUT TO DRIVE HOME THE BULGE POPPED EXPOSING BROKEN PLY CORDS AND TREAD SEPARATION.
ON OCTOBER 9, 2009, PURSUANT TO FORD RECALL 05S28, A LOCAL FORD DEALER, DAVIES FORD, CHARLEROI, PENNSYLVANIA, INSTALLED A WIRING HARNESS ON MY VAN. ONLY FIVE DAYS LATER, WHILE MY VAN WAS PARKED, THE ENGINE TURNED OFF,AND THE KEYS REMOVED FROM THE IGNITION, MY VAN CAUGHT FIRE AND WAS COMPLETELY DESTROYED. AN EXPERT INSPECTED THE VAN AND DETERMINED THAT THE FIRE STARTED IN THE EXACT LOCATION WHERE THE MASTER CYLINDER AND SCDS WERE INSTALLED AND THAT THE FIRE WAS CAUSED BY A DEFECTIVE SCDS. THE DEALER PROMISED TO GIVE MA A VAN OF EQUAL VALUE OR AN AMOUNT OF MONEY EQUALING THE VAN'S VALUE, BUT AFTER TWO YEARS, RENEGED ON ITS PROMISE. FORD MOTOR COMPANY WILL NOT TALK WITH ME. I HAVE BEEN DEPRIVED OF THE USE OF THE VAN SINCE OCTOBER 14, 2009 AND HAVE INCURRED HUGE EXPENSES FOR TRANSPORTATION, STORAGE, TRAUMA AND EMOTIONAL DISTRESS. I REALIZE THAT I AM ONLY ONE OF THOUSANDS OF FORD VEHICLE OWNERS WHO HAVE SUFFERED THE LOSS OF THEIR VEHICLES BECAUSE OF THIS DEFECTIVE SCDS, AND I WOULD APPRECIATE IT IF YOU WOULD CONDUCT AN INVESTIGATION OF MY LOSS AND THEN INFORM ME OF YOUR FINDINGS.. THANK YOU, [XXX] INFORMATION REDACTED PURSUANT TO THE FREEDOM OF INFORMATION ACT (FOIA), 5 U.S.C. 552(B)(6). *TR
TL* THE CONTACT OWNS A 1993 FORD ECONOLINE. THE CONTACT STATED THAT WHILE DRIVING AT 35 MPH, THE GEAR BOX FRACTURED FROM THE FRAME. IN ADDITION, THE CONTACT STATED THAT THE STEERING WHEEL SEIZED. THE VEHICLE WAS TOWED TO THE CONTACTS RESIDENCE. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS NOT NOTIFIED OF THE FAILURE. THE APPROXIMATE MILEAGE WAS 110,000.
VEHICLE SWAYS AND DRIFTS ON ROAD. EXCESSIVE FREE PLAY IN POWER STEERING GEAR BOX. STEERING GEAR BOX WAS REPLACED BUT WITH ORIGINAL EQUIPMENT CONDITION IS THE SOME. WHY WAS GEAR BOX NOT RECALLED WHEN TIRES WERE RECALLED? IS THERE AN UPGRADED PART THAT WILL SOLVE THE PROBLEM? ( SEE NHTSA REFERENCE #10382765) ALSO FORD TRUCK ENTHUSIASTS FORUMS - STEERING PROBLEMS. *TR
DRIVING HOME FROM SHOPPING I BACKED OUT OF A PARKING SPACE AND HEARD A LOUD POPPING SOUND UPON INSPECTION THE 2 MOUNTING BOLTS HOLDING THE GEARBOX TO THE FRAME RAIL HAD SHEARED OFF AND THE 3RD ONE HAD RIPPED THROUGH THE FRAME RAIL COMPLETELY AND DROPPED THE GEARBOX HAD TO HAVE IT TOWED HOME UPON FURTHER INSPECTION THERE ARE STRESS CRACKS AROUND THE MOUNTING HOLES FOR THE GEARBOX BOLTS. *TR
TL*THE CONTACT OWNS A 1993 FORD E350. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY LESS THAN 60 MPH THE VEHICLE WOULD FISH TAIL CAUSING THE VEHICLE TO SWAY LEFT AND RIGHT. THE VEHICLE WAS INSPECTED BY A DEALER WHO ADVISED HIM THAT IF EVERYTHING THAT WAS CONNECTED TO THE STEERING COLUMN WERE REPAIRED IT MAY REMEDY THE FAILURE. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS APPROXIMATELY 85,000. UPDATED 7/18/14*CN *TR
TL*THE CONTACT OWNS A 1993 FORD ECONOLINE. THE CONTACT STATED THAT WHILE DRIVING APPROXIMATELY 5 MPH AND MAKING A RIGHT TURN THEY HEARD A LOUD SNAPPING NOISE. THE STEERING WHEEL BECAME VERY LOOSE AND CONTINUED TO MOVE INSTEAD OF STOPPING AT A SPECIFIC POINT. NO WARNING LIGHTS APPEARED ON THE INSTRUMENTAL PANEL. THE VEHICLE WAS UNABLE TO BE DRIVEN. THE VEHICLE WAS TOWED AND INSPECTED BY A INDEPENDENT MECHANIC WHO STATED THAT THE STEERING GEAR BOLTS SNAPPED AND NEEDED TO BE REPLACED. THE VEHICLE WAS NOT REPAIRED. THE FAILURE MILEAGE WAS APPROXIMATELY 168,000. UPDATED 03/24/11*LJ UPDATED 12/14/11 *CN
THE VEHICLE WAS BEING DRIVEN ON THE HIGHWAY, AND IT CAUGHT FIRE. THE POLICE AND THE FIRE DEPARTMENT WERE PRESENT AT THE SCENE, BUT AT THE TIME THE INCIDENT TOOK PLACE, IT WAS A COMPLETE LOSS. *TR
I WAS DRIVING EAST, JUST PAST MONROE, LA, ON I-20 JUST PRIOR TO MILE MARKER 126 WHEN THE RIGHT PASSENGER TIRE CAME OFF MY E150 1993 FORD VAN. I WAS ABLE TO MAINTAIN CONTROL OF THE VAN TO GET IT OFF THE ROAD. THANKFULLY, THE RIM/TIRE, AND BRAKE CALIPER DID NOT HIT A VEHICLE; I FOUND IT ABOUT A HALF MILE PRIOR TO WHERE I WAS ABLE TO GET THE VAN STOPPED. I THOUGHT I A BLOWOUT HAD OCCURRED BUT WHEN I LOOKED, THERE WAS NO RIM OR TIRE ON THE VAN. I BOUGHT THE VAN NEW IN LATE 1992 AND HAVE MAINTAINED IT WELL THROUGHOUT ITS LIFETIME. HOW CAN THIS HAPPEN? JUST PRIOR TO GETTING TO MONROE, THERE WAS A WOBBLE IN THE STEERING LIKE A BIG GUST OF WIND HAD HIT IT OR I HAD STRUCK A RECAP. I GOT OUT AND CHECKED BUT FOUND NOTHING UNUSUAL. I DROVE ON TO MONROE AND ATE LUNCH AT CHILI'S. SHORTLY AFTER GETTING BACK ON I-20 IS WHEN THIS EPISODE HAPPENED. A LOT OF PEOPLE COULD HAVE BEEN INJURED OR KILLED. WEATHER WAS CLEAR WITH LIGHT BREEZE AND NO RAIN. THIS IS THE FIRST TIME THIS HAS HAPPENED TO ME. THE VAN WAS TOWED BY AAA BY BEARS TO HIXSON FORD IN MONROE, LA FOR REPAIR WHERE IT IS NOW WAITING. THE WHEEL WELL, PASSENGER DOOR AND VARIOUS TRIM ITEMS WERE ALSO DAMAGE DUE TO THE WHEEL COMING OFF AND HAVING IT TOWED. *TR
WIFE WAS DRIVING VAN OUT OF DRIVEWAY HEARD A LOUD SNAPPING SOUND AND SHE LOST STEERING AND BRAKES WENT OUT SHE DID NOT MAKE IT TOO THE ROAD I WENT OUT AND LOOKED AT VAN AND THE STEERING BOX BOLTS HAD SNAPPED OFF CAUSING THE STEERING BOX TOO HIT BRAKE LINE VAN WAS TOWED TO REPAIR SHOP REPAIRS ARE PENDING. *TR
GOT IN MY VAN STARTED DOWN STREET AND SMELT SMOKE WENT AROUND BLOCK INSIDE OF VAN FULL OF SMOKE STOPPED VAN AND SHUT IT OFF GOT OUT OF IT AND CALLED FOR FIRE DEPT AND NEIGHBOR CALLED TO BY TIME FIRE DEPT CAME MY VAN WAS FULLY ON FIRE MELTED SIDING ON HOUSE I WAS NEXT TOO..SMOKE AGGRAVATED MY ASHTMA AND HAD TO DO MY NEBULIZER............NOW I HAD A RECALL AND SUPPOSABLY IT WAS CORRECTED BUT MY VAN STILL CAUGHT FIRE...I DON'T HAVE FIRE COVERAGE WHAT IS MY NEXT THING I CAN DO TO GET COMPENSATION....IF MY RECALL WAS FIXED WHY DID IT STILL CATCH FIRE....HAD NO PROBLEMS WITH VAN BEFORE ALL HAPPENED...ONLY WORK DONE ON IT WAS FOR THE RECALL... *TR
SPEED CONTROL DEACTIVACTION SWITCH. *TR
NON RESPONSIVE TO RECALL FIX. *TR
FORD RECALL 05S28 OF THE SPEED CONTROL DEACTIVATION SWITCH. I WAS CONTACTED BY FORD TO BRING MY E-150 VAN IN FOR A RECALL ON MY SCDS. I TOOK THE VEHICLE IN QUESTION TO WADE FORD IN SMYRNA, GA. 30080. THEY DISCONNECTED THE SCDS AND SAID THAT THEY DIDN'T HAVE THE PARTS TO FIX THE PROBLEM AND IT WOULD BE OCT. BEFORE THEY WERE AVAILABLE. I HAVE WAITED PATIENTLY WHILE FORD TOOK THEIR TIME TO CORRECT THE PROBLEM. I HAVE CALLED EVERY MONTH TO GET MY VEHICLE REPAIRED AND FINALLY ON FEB. 29, 2008 I WAS TOLD BY DAVE CHANCE A SERVICE ADVISOR THAT THEY FINALLY HAD THE PARTS TO MAKE THE NECESSARY REPAIRS. THEY ASSURED ME THAT THEY HAD THE PARTS TO MAKE THE REPAIR AND I SET UP AN APPOINTMENT TO HAVE THE REPAIR DONE AND THEY TOLD ME THAT IT WOULD TAKE 1 TO 2 HOURS TO DO. MY APPOINTMENT WAS FOR MARCH 4, 2008 AT 8:00 AM. I ARRIVED AT THE SERVICE DEPARTMENT AT 7:45 AM AND WAS CHECKED IN AND TOLD THAT I COULD WAIT IN THEIR WAITING ROOM TILL THEY WERE DONE. AT 8:55 AM THE SERVICE ADVISOR DAVE CHANCE CAME IN TO TELL ME THAT HE WAS SORRY THAT THEY DIDN'T HAVE THE PARTS IN TO FIX THE SCDS AND THERE WAS NOTHING THAT THEY COULD DO. I WAS VERY UPSET WITH THESE PEOPLE AS I WAS GIVEN THE IMPRESSION AND THE NOTICE THAT THEY COULD REPAIR MY SCDS AT THIS TIME. I TOLD THEM THAT MY TIME WAS AS IMPORTANT TO ME AS THEIR TIME WAS TO THEM. THEY SAID THAT THEY WERE SORRY FOR THE INCONVENIENCE THAT IT CAUSED ME, AND WHEN I TOLD THEM THAT THEY SHOULD PAY ME THE SAME HOURLY RATE THAT THEY CHARGE TO WORK AN MY VEHICLE THEY SAID THAT THEY WOULD CHANGE MY OIL FOR ME FREE OF CHARGE. I FELT THAT THIS WAS A SLAP IN THE FACE AND THAT THEY COULD CARE LESS ABOUT MY TIME. *TR
RECEIVED RECALL 1993 E-350 ECONOLINE 08S01 MADE APPOINTMENT EVERY FORD FAYETTE, AL. LEFT IT OVER NIGHT TO BE WORKED ON THE NEXT DAY. CALLED 4:30PM BEFORE CLOSING TO SEE IF IT WAS DONE. TOLD THEY WOULD CALL ME BACK IT WAS NEXT THEN THEY CALLED AND SAID THEY DIDN'T HAVE A PART & DIDN'T KNOW WHEN ONE WOULD BE AVAILABLE. WE WASTED 8 GALLONS OF GAS AND THE RECALL PART IS STILL NOT BEEN REPLACED. THEY CLAIM NO ONE HAS THE PART FOR THE ECONOLINE. I CALLED THE 1-800 NUMBER IN THE LETTER BUT IT IS ONLY A VOICE MAIL BOX AND IT DIRECTS TO MAKE THE CALL OVER AGAIN. *TR
TL*THE CONTACT OWNS A 1993 FORD ECONOLINE. THE CONTACT RECEIVED A RECALL NOTICE IN NOVEMBER OF 2007 FOR THE VEHICLE SPEED CONTROL: CRUISE CONTROL. THE VEHICLE WAS REPAIRED, BUT THE DEALER REISSUED A NEW RECALL NOTICE IN FEBRUARY OF 2008. THERE HAD BEEN NO FAILURE TO DATE. THE RECALL NUMBER WAS UNKNOWN. THE CURRENT MILEAGE WAS 309,997.
TL*THE CONTACT OWNS A 1993 FORD E350. THE CONTACT RECEIVED A RECALL NOTICE FOR NHTSA CAMPAIGN ID NUMBER 07V336000 (VEHICLE SPEED CONTROL) AND FORD RECALL NUMBER 05S28 IN AUGUST OF 2007. HE CALLED FORD SEVERAL TIMES AND THEY STATED THAT THE PARTS WOULD BE AVAILABLE IN MID'DECEMBER OF 2007 AND THEN IN JANUARY OF 2008. THE DEACTIVATION SWITCH WAS DISCONNECTED. THERE HAD BEEN NO FAILURE TO DATE. THE CURRENT MILEAGE WAS 184,000.
1993 FORD E-350 TIRE BLEW OUT CAUSING THE CONSUMER TO LOSE CONTROL OF THE VEHICLE. WHEN HE LOST CONTROL HE DROVE OFF THE ROADWAY AND HIT THE MEDIAN WALL. *KB (OHIO CRASH TRAFFIC CRASH REPORT)*JB
TL*THE CONTACT OWNS A 1993 FORD ECONOLINE. THE CONTACT RECEIVED A RECALL NOTICE IN AUGUST OF 2007 FOR THE VEHICLE SPEED CONTROL SWITCH. SHE SCHEDULED AN APPOINTMENT TO HAVE THE VEHICLE REPAIRED, BUT IT CAUGHT FIRE BEFORE THE APPOINTMENT DAY. THE VEHICLE WAS COMPLETELY DESTROYED. THE CONTACT FILED A COMPLAINT WITH THE MANUFACTURER. THE POWERTRAIN AND RECALL NUMBER WERE UNKNOWN. THE CURRENT AND FAILURE MILEAGES WERE 103,000.
TL*THE CONTACT OWNS A 1993 FORD ECONOLINE. WHILE DRIVING UPHILL AT 10 MPH, THE CONTACT NOTICED SMOKE RISING FROM THE HOOD. NHTSA RECALL NUMBER 94V128000 (INTERIOR LIGHTING) WAS REFERENCED. THE VEHICLE ERUPTED INTO FLAMES AND MELTED THE SIDING OF A HOUSE. THE FIRE DEPARTMENT EXTINGUISHED THE FLAMES AND A POLICE REPORT WAS FILED. THE CONTACT HAS NOT SPOKEN TO THE DEALER. THERE WAS NO CURRENT MILEAGE BECAUSE THE VEHICLE WAS DESTROYED. THE FAILURE MILEAGE WAS 80,000. UPDATED 08/13/08 *BF THE CONSUMER STATED A WEEK PRIOR, THE CRUISE CONTROL STOPPED WORKING. THE CONSUMER REPLACED THE FUSE, BUT THE CRUISE CONTROL STILL DIDN'T WORK. UPDATED 08/13/08. *JB
TL*THE CONTACTS OWNS A 1993 FORD E150. WHILE DRIVING 45 MPH WITH THE CRUISE CONTROL ACTIVATED, THE VEHICLE FAILED TO STOP WHEN THE BRAKE PEDAL WAS DEPRESSED. THE CONTACT STATED THAT HE HAD TO SHIFT THE VEHICLE INTO NEUTRAL AND THEN APPLY THE BRAKES FOR THE VEHICLE TO STOP. THE DEALER HAS NOT INSPECTED THE VEHICLE. THE FAILURE MILEAGE WAS 127,000 AND CURRENT MILEAGE WAS 128,000. UPDATED 01-16-08. *KB THE MECHANIC STATED THE PROBLEM WAS DUE TO CRUISE CONTROL FAILURE. THE CONSUMER HAS CRASHED INTO MAILBOXES CAUSING DAMAGE TO THE VEHICLE. THE CONSUMER HAS SINCE SOLD THE VEHICLE. UPDATED *JB
TL*THE CONTACT OWNS A 1993 FORD E350. THE CONTACT RECEIVED NHTSA RECALL NOTICE NUMBER 07V336000 (VEHICLE SPEED CONTROL). THE NOTICE ADVISED HIM TO CALL 1-800-444-3311 FOR A LIST OF LOCAL DEALERS. WHEN HE CALLED, THE PHONE RANG TWICE AND GAVE A BUSY SIGNAL. WHEN HE CALLED 1-800-392-3673, HE WAS INFORMED THAT THEY WERE UNABLE TO ASSIST WITH MOTORHOMES. THE CONTACT HAS BEEN UNABLE TO MAKE AN APPOINTMENT OR FIND A DEALER. THERE HAD BEEN NO FAILURE TO DATE. THE CURRENT MILEAGE WAS 39,000.
TL*THE CONTACT OWNS A 1993 FORD ECONOLINE. WHILE DRIVING 35 MPH, THE CONTACT NOTICED SMOKE COMING FROM THE HOOD. WHEN HE RAISED THE HOOD, THE VEHICLE IGNITED. THE DEALER INSPECTED THE VEHICLE AND STATED THAT THE DEACTIVATION SWITCH MALFUNCTIONED AND CAUSED THE VEHICLE TO CATCH FIRE. THE CONTACT RECEIVED FORD RECALL NOTICE NUMBER 05S28 ON AUGUST 29, 2007. THE VIN, ENGINE SIZE, NUMBER OF CYLINDERS, DEALER INFORMATION, AND MILEAGES WERE UNAVAILABLE.
FORD RECALL #05S28 INDICATES A POTENTIAL FIRE HAZARD IN MY "SPEED CONTROL DEACTIVATION SWITCH" WHICH MAY LEAK CAUSING A UNDERHOOD FIRE. FORD WANTS TO PUT A FUSE IN THE WIRING HARNESS TO PREVENT THIS FROM HAPPENING. WHY WOULD FORD NOT WANT TO CHANGE THE SCDS SWITCH THAT MIGHT BE LEAKING INSTEAD? *TR
TL*- THE CONTACT STATED THAT THE 1993 FORD ECONOLINE VAN CAUGHT ON FIRE WHILE SITTING IN THE DRIVEWAY. WHILE IN HIS VEHICLE SLEEPING ABOUT 4:00 AM THE NEIGHBORS KNOCK ON THE VAN TO INFORM THE CONTACT THAT THE VEHICLE WAS ON FIRE UNDER THE HOOD. HE STATED THAT THE ENTIRE VAN WAS DESTROYED BY THE FIRE. THE CONTACT STATED THAT THE FIRE DEPARTMENT CAME AND PUT OUT THE FIRE. THE CONTACT DROVE THE VEHICLE HOME, AND THERE WAS NO INDICATION THAT THE VEHICLE HAD ANY TYPE OF PROBLEMS. THE CURRENT AND FAILURE MILEAGE WERE BOTH 128000 . *AK
1993 FORD E150 VAN FRAME CRACKED AROUND BOLT HEADS THAT HOLD STEERING BOX ON, CAUSING ERRATIC STEERING
I WAS DRIVING AT 60 MPH WHEN I BEGAN DECELERATING AND REALIZED ENGINE HAD SHUT OFF. I COASTED TO A STOP. I WAS GETTING TOOLS TO CHECK RELAYS WHEN I NOTICED FIRE AT REAR WHEEL, DRIVER SIDE, AT GAS TANK. CALLED CLOSEST FIRE DEPARTMENT. 6/9/06. PARKING BRAKE LINE ON FIRE WITH ABS LINE. HAD WIRING REPAIRED. JULY 16,2006 BRAKES FELT LIKE THEY WERE LOCKING, REAR WAS SMOKING AGAIN, LOOKED LIKE FIRE AT GAS TANK. JULY 17 HAD MECHANIC CHECK ALL BRAKES WHICH WERE EXCELLENT EXCEPT PARKING BRAKE LINE BENT, BUT RELEASED. JULY 19, BRAKES LOCKING UP A LITTLE. JULY 20, COULDN'T DRIVE WITHOUT REVERSE/FORWARD AND STILL DIDN'T WANT TO GO. I SELL ICE CREAM TO LITTLE CHILDREN WHILE MY VAN IS RUNNING. PARKING BRAKES WORK BUT WON'T RELEASE FULLY. APPEARED TO BE VINYL LINING AT FLOOR LEVEL INTERFERING, BUT MAY HAVE BEEN WIRING. HAD A SECOND FIRE ON GROUND BATTERY TERMINAL AND INSIDE HOOD ON JUNE 16,2006 CALLED FIRE DEPARTMENT. DON'T KNOW CAUSE. REPLACED BURNED WIRING ONLY. ALL ELSE WORKED. ALSO, IT APPEARS THE LEAKY FILLER HOSE WAS NEVER REPLACED ON THIS VAN. INTERIOR LIGHT HAD FIRE PATTERN WHEN BOUGHT SECOND HAND. I WAS NOT AWARE THERE WAS A RECALL. *NM
A FEW DAYS AGO I WAS DRIVING MY VEHICLE AND NOTICED A BURNING SMELL I CHECKED ALL OF THE FUSES FIRST AND THERE WAS NO PROBLEM. FINALLY I DROVE THE VAN AGAIN AND NOTICE SMOKE COMING FROM THE DOME LIGHT AT THAT POINT I REMOVED THE LIGHT ITSELF AND NOW I HAVE PROBLEMS WITH THE LIGHTING. I DID LOOK UP RECALL DEFECTS FOR 93 VEHICLES WHICH STATED THAT THE INTERIOR LIGHTING WAS A DEFECT. I CALLED FORD AND THEY SEEM TO HAVE NO KNOWLEDGE OF RECALL. THIS RECALL IS ON YOUR SITE AS ID # 94V128000 AND THE DEFECT IS 6088 INTERIOR LIGHTING. *JB
DT: THE CALLER SAID THERE WERE RECALLS 93V1000000 CONCERNING FUEL TANK AND 94V128000 CONCERNING INTERIOR LIGHTING , BUT THIS VEHICLE WAS NOT INCLUDED. SHE HAD THE WORK DONE ON THE VEHICLE. THE CALLER SAID VEHICLE WOULD NOT START, AND THE DOME LIGHT WAS BLOWING FUSES AND MELTING. DEALER AND MANUFACTURER SAID THE CALLER'S VEHICLE WAS NOT INCLUDED IN THE RECALLS. *AK
TOGGLE SWITCH ON SUNROOF HAS ALREADY BEEN REPLACED ONCE AND NOW IT HAS GONE OUT AGAIN. DOES NOT STOP ON ITS OWN FOR OPEN AND CLOSE. I DON'T FEEL I SHOULD HAVE TO PAY FOR SOMETHING THAT CONTINUES TO BREAK.
DT: FORD, ECONLINE 150 CONVERSION VAN 1993, VEHICLE CAUGHT ON FIRE. CONSUMER BELIEVED IT WAS DUE TO THE CRUSE CONTROL, CONSUMER WAS DRIVING AND SAW SMOKE COMING FROM UNDER THE HOOD, CONSUMER DIALED 911. WHEN FIRE DEPTPARTMENT CAME THEY HAD TO CUT AROUND THE LIFT LEVER OF THE HOOD, WHEN THE HOOD WAS REMOVED THERE WERE FLAMES COMING FROM THE MOTOR, THE WHOLE VEHCILE BURST INTO FLAMES, THE WHOLE ENGINE DASHBOARD MELTED. *AK
I OWN A FORD ECOLINE 150 FAMILY VAN (CUSTOM MADE). WELL JUST LAST WEEK IT CAUGHT ON FIRE WHILE MY HUSBAND WAS DRIVING ON HE HIGHWAY. HE HAD THE CRUISE CONTROL, A.C. AND THE RADIO ON. I HAS NEVER HAPPENED TO US BEFORE. I DON'T KNOW IF IT DID TO THE PRIOR OWNERS. NEEDLESS TO SAY THAT WHEN HELP ARRIVED IT WAS TO LATE THE VAN WAS TOTALED.
FROM THE DATE THE CONVERSION VAN WAS PURCHASE, THE CONSUMER WAS HAVING AN ON GOING PROBLEM WITH THE STEERING. THE VAN WOULD NOT DRIVE STRAIGHT, IT WANDERED ALL OVER THE ROAD. OVER THE YEARS IN AN ATTEMPT TO CORRECT THIS PROBLEM THE BALL JOINTS AND STEERING GEAR HAS BEEN REPLACED. THE PROBLEM STILL EXISTED. *JB
I HAVE A 1993 FORD E150 CONVERSION VAN WITH AT, ABS,PS, PW, PL, TV, VCR, AND TYPE N ENGINE (V8 5.0). I WENT TO FILL UP WITH GASOLINE AND IT APPEARS THAT THE VENT PIPE LEAKS. HAS THIS PROBLEM BEEN IDENTIFIED BY OTHER OWNERS? *JB
WHILE TURNING IN A PARKING LOT SHIFTER DISCONNECTED, CAUSING THE VEHICLE NOT TO SHIFT OUT OF GEAR. *AK IT WAS LATER DETERMINED THAT THE SHIFT LINKAGE ROD SNAPPED APART INSIDE THE STEERING COULMN. THE CONSUMER PURCHASED THE UPDATED PARTS AND INSTALLED IT HIMSELF. *NM
WHILE DRIVING AT NORMAL SPEED CONSUMER HEARD A LOUD NOISE, SOUNDED LIKE IT WAS COMING THROUGH THE FONT END. VEHICLE WAS TAKEN TO THE DEALER, AND TECHNICIAN INDICATED THAT FRAME CRACKED AT THE STEERING BOX LEFT SIDE. *AK
WHILE DRIVING AT ANY SPEED WATER AND ANTI FREEZE LEAKED INTO THE PASSENGER COMPARTMENT. ALSO, VEHICLE INTERMITTENTLY STALLED WHEN TURNING CORNERS. *AK
A/C AND HEATER BLOWER SWITCHS ARE TO LIGHT FOR THE APLICATION ELETRICAL SYSTEM DRAWS TO MANY AMPS. BURNS UNDERDASH WIRING AND WILL CAUSE FIRES. MARKIII AND FORD BOTH USE THE SAME MANUFACTURE SWITCHS FRO THE INDAK CORP.*AK
GAS TANK FELL OF VEHILCE. DEALER NOTIFIED.*AK
1993 FORD E-150 VAN LEAKS FUEL FROM TANK (NOT FILLER NECK) DURING FILLUP. UNABLE TO COMPLETELY FILL TANK BECAUSE OF THIS PROBLEM.
CONSUMER IS HAVING PROBLEM LOCATING A DEALERSHIP THAT CAN DO THE RECALL FOR THE LAMP AND SOCKET 94 V 128 000 ON A CONVERSION VEHICLE. CONSUMER CONTACTED THE MANUFACTURER, BUT THEY ARE NO HELP. TS *JG
THE FRONT END OF THE VEHICLE DEVELOPED VIBRATION DUE TO CRACKED ROTORS. THE BRAKE PADS WERE ALSO CRACKED IN HALF. *YH THE BRAKE PADS WERE CRACKED IN HALF BUT WERE NOT WORN TO THE POINT OF NEEDING REPLACEMENT. HOWEVER NEW BEARINGS AND SEALS WERE REPLACED. PHOTOS ATTACHED. *TT
CONSUMER STATES THE STEERING GEAR BOX COLLAPSE. PLEASE PROVIDE FURTHER INFORMATION.. TS
THE THREE BOLTS THAT MOUNT THE STEERING BOX BROKE AND THE FRAME HAS MULTIBLE CRACKS,THE BOLTS SHOW NO SIGN OF WEAR AS IF LOOSE, BUT DO LOOK LIKE THEY MIGHT HAVE BEEN OVER TIGHTENED. THIS HAPPENED SUDDENLY AND RESULTED IN NO CONTROL OF THE VAN.*AK
OUR VAN WAS MODIFIED IN DECEMBER, 2000, WITH A RAISED ROOF AND EXTENDED DOORS TO ALLOW ACCESSABILITY FOR OUR HANDICAPPED SON. WE DISCOVERED AROUND JULY, 2002, THAT THE COMPANY PERFORMING THE MODIFICATION HAD NOT INSTALLED A REINFORCED STEEL CAGE OR USED A RAISED FIBERGLASS ROOF ALREADY REINFORCED. THIS IS A MAJOR OMISSION THAT COULD CAUSE SERIOUS INJURY IN THE EVENT OF A ROLLOVER OR OTHER SERIOUS INCIDENT; A MAJOR SAFETY ISSUE. WE HAVE NOTIFIED THE COMPANY ON JULY 29, 2002OF OUR CONCERNS BUT HAVE NOT RECEIVED A RESPONSE AS OF THIS DATE. THE COMPANY PERFORMING THE MODIFCATION IS ACCESSABILITY SPECIALISTS, INC., 1815 CORPORATE SQUARE BOULEVARD SUITE 200, JACKSONVILLE, FLORIDA 32216. THE COMPANY PRESIDENT IS WEST WESTMORELAND. WE HAVE FILED A FORMAL COMPLAINT WITH NMEDA (WEB SITE WWW.NMEDA.ORG) OF WHICH THE COMPANY IS A MEMBER.*AK
TREAD SEPARATION FROM BODY OF TIRE AT SIDEWALL. MODERATE VIBRATION PROIR TO FAILURE. TIRE REMOVED FROM SERVICE BEFORE IT CATASTROPHIC FAILURE.*AK
THE INNER WORKINGS OF THE KEYHOLE WITHIN IGNITION IS MISALIGNED. THE KEY CANNOT START THE VEHICLE. HAVE BEEN STRANDED TILL AFTER COUNTLESS TRIES, ALL OF A SUDDEN IT WILL MOVE AND THE IGNITION FINALLY UNLOCK. I ALWAYS HAVE THE BEEPING GOING ON IF THE DOOR IS OPEN, EVEN WITH NO KEY IN IGNITION. THIS CAN ONLY BE SILENCED BY WIGGLING THE IGNITION (WITHOUT A KEY IN IT) I AM VERY MUCH AFRAID THE IGNITION IS GOING TO SEPARATE FROM STEERING COLUMN AND JUST FALL OUT! THAT WOULD LEAVE ME NO WAY TO START THE VEHICLE AND GET HOME! NLM
CONSUMER WAS PARKING AND STRAIGHTENING VEHICLE OUT WHEN IT SUDDENLY ACCELERATED INTO GARAGE. VEHICLE HAD BEEN MODIFIED TO A HANDICAP VAN.*AK
NO FAULT CODES COULD BE FOUND AFTER INCIDENT BUT PROBLEM PERSISTS. NO SAFETY DEFECT STATED.
RUBBER HOSE ATTACHMENT TO INLET PIPE TO METAL FUEL FILLER TUBE WAS CORRODED, AND DEVELOPED A CRACK WHICH CAUSED A FUEL LEAKAGE WHEN TANK WAS BEING FILLED.*AK
THE DRIVERS SIDE REAR TIRE EXPERIENCED TREAD SEPARATION, ALSO THE THE PASSENGER REAR TIRE EXPERIENCED TREAD SEPARATION THE VERY NEXT DAY, THE TIRES WERE DAYTONA F235/75R/15, HOWEVER CONSUMER WAS INFORMED THAT THE TIRES WERE MADE BY FIRESTONE, CONSUMER HAS SINCE REPLACED ALL FOUR TIRES.*JB
THE DRIVERS SIDE REAR TIRE EXPERIENCED TREAD SEPARATION, ALSO THE THE PASSENGER REAR TIRE EXPERIENCED TREAD SEPARATION THE VERY NEXT DAY, THE TIRES WERE DAYTONA F235/75R/15, HOWEVER CONSUMER WAS INFORMED THAT THE TIRES WERE MADE BY FIRESTONE, CONSUMER HAS SINCE REPLACED ALL FOUR TIRES.*JB
ON AT LEAST 4X THE IGNITION CUT OF AT HIWAY SPEEDS.MAGARITY. *AK
FUEL SMELL APPEARED SOON AFTER FILLING VEHICLE. VEHICLE WAS SERVICED, TECHNICIAN STATED VENT AND FILLER HOSE NEEDED TO BE REPLACED. PLEASE PROVIDE FURTHER INFORMATION.*AK
WHILE CHANGING MY OIL I HAD NOTICED THAT THE POWER STEERING HOSE WAS IN CONTACT WITH THE FRAME OF THE VEHICLE AND WEAR MARKS WERE EVIDENT. IF A PIECE OF RUBBER HOSE WAS NOT PLACED AROUND THE HOSE FAILURE OF THE HOSE WOULD HAVE TAKEN PLACE.*AK
WE HAE EXPERIENCED PLY SEPARATIONS ON AT LEAST TWO TIRES ON THIS VAN FOR THE PAST THREE YEARS. AN INVESTIGATION INTO THE CUASE OF THIS PROBLEM WHOULD BE INITIATED.*AK (TIRESIZE: 245/75-R16)( DOT NUMBER: TIRE SIZE: 245/75-R16 )
LEFT MEMPHIS, TN FOR OUT OF TOWN TRIP ON 4/12/01. ALL FOUR TIRES ROTATED AND BALANCED BY LOCAL FIRESTONE DEALER 5 DAYS BEFORE TRIP (ERIC PH 901-323-2627). STAYED MURPHREESBORO, TN OVERNIGHT. STARTED DRIVING 9AM 4/13/01, GOT TO MONTEAGLE, TN GOING UP HILL, THUMP, THUMP, THUMP. LOOKED - PEACH SIZE BULGE, INSIDE RIGHT FRONT TIRE, AT POINT WHERE SIDE WALL MEETS TREAD. PUT FOUR NEW TIRES ON AT MONTEAGLE DUE TO SAFETY CONCERNS. GOT BACK TO MEMPHIS, LOCAL FIRESTONE DEALER, ERIC, CONFIRMED TREAD SEPARATION AS DID INDEPENDENT TIRE DEALER, GATEWAY TIRE. LOCAL DEALER OFFERED CREDIT FOR UNUSED TREAD TOWARD PURCHASE OF ONE REPLACEMENT TIRE. I DECLINED OFFER. CALLED FIRESTONE RECALL HOTLINE, PH 800-465-1904, 04/16/01, EXPLAINED PROBLEM, MY TIRES P235/75R15 105S MTS, DOT # VDHL AWR 447, WILDERNESS HT, WOMAN SAID NOTHING THEY COULD DO BECAUSE TIRE NOT ON RECALL LIST. I ASKED IF SHE WANTED MY NAME, ADDRESS AND INFORMATION SO THEY COULD CONTACT ME IF NEEDED OR TO REPORT PROBLEM AND SHE SAID NO. PLEASE CALL, WOULD LIKE TO KNOW WHAT TO DO NEXT, WOULD BE HAPPY TO DISCUSS IN FURTHER DETAIL. I STILL HAVE ALL FOUR TIRES.*AK (DOT NUMBER: VDHLAWR447 TIRESIZE: P235/75R15)
THE RIGHT REAR TIRE HAD IT'S STEEL BELTS PROTRUDING OUT OF THE SIDEWALL UNDER THE TREAD CAP, THE TIRES ALSO HAVE POOR TRACTION IN RAIN, SNOW OR MUD UPON BRAKING (FIRESTONE WILDERNESS AT). NLM
WHEN FILLING FUEL TANK, BEFORE TANK IS FILLED , FUEL RUNS OUT OF TANK.*AK
PARKING BRAKE SLIPS OFF ON ANY LEVEL SURFACE. RACHET MECHANISM NEEDED TO BE REPLACED. THIS IS WAS 2ND TIME IT HAD HAPPENED. *AK
THREE TIMES THE LEFT FRONT INNER WHEEL BEARING HAS DISINTEGRATED ALLOWING ROTOR TO FALL DOWN ON SPINDLE, WITH NO INDICATION OF BEARING FAILURE, NO NOISE WHATSOEVER.THIS MOST RECENT INCIDENT TIRE WHEEL ROTOR CAME COMPLETELY OFF SPINDLE AT 70 M.P.H. THE OUTER BEARING STILL FULL OF GREASE . INDICATION THAT THERE IS INSTANTANIOUS DISCENERGRATION OF INSIDE BEARING. I BELIEVE SPINDLE WAS TURNED TO SMALL BY A FEW THOUSANDS ALLOWING RACE TO BREAK LOOSE. I AM BLESSED TO HAVE WALKED AWAY FROM THIS ENGNEERING DIASTER CALLED FORD ECONOLINE. I AM 53 YEARS OLD @ HAVE HAD MORE PROBLEMS WITH THIS VAN THAN ALL OF THE OTHER VEHICLES I HAVE EVER OWNED.*AK
REPAIR SHOP USED SAID MANIFOLD WAS MADE DEFECTIVE--FIRE HAZARD --I CALLED CUSTOMER SEVICE--TOLD THEY KNOW OF NO PROBLEMS--PARTS STORE SAID THIS IS COMMON WITH THIS MOTOR---I TALKED TO FORD REPS. AT THE CHICAGO CAR SHOW THEY SAID TO CALL CUST. SERVICE....I BUY MOPAR PRODUCTS NOW.*AK
TIRES CAME APART BY THE LINE AROUND IT, HAD TO REPLACE THEM. *AK (TIRESIZE: 17)( DOT NUMBER: TIRE SIZE: 17 )
VEHICLE FILLED WITH FUEL & PARKED ON AN INCLINE, AND FUEL WOULD THEN LEAK OUT. DOES NOT HAPPEN ON STRAIGHT AWAY. SOMETIMES FUEL WOULD SPLASH OR SLOSH OUT WHEN COMING TO A QUICK STOP. HAD NOT TAKEN TO DEALER AS OF YET.*AK
FRONT BALL JOINTS REPLACED TWICE. NEEDED TO BE DONE AGAIN. ALSO, PARK BRAKE REPLACED 3 TIMES. *AK
STARTED VEHICLE & SHIFTED INTO REVERSE WHEN VEHICLE ACCELERATED BACKWARDS SUDDENLY. HAD FOOT ON BRAKES AT THE TIME. BRAKES FAILED TO STOP VEHICLE. WENT THROUGH NEIGHBOR'S GARAGE. NO INJURIES. *AK
GOODYEAR WRANGLER HT TIRES (P225 75 R15) EXPERIENCED STEEL BELT SEPARATION, CONSUMER IS REQUESTING REIMBURSEMENT. *SLC
ONE OF THE FIRESTONE STEELTEX R4S (P235/75R15) EXPERIENCED TREAD SEPARATION AND NOISE FROM THE RIGHT REAR TIRE, THE CONSUMER REPLACED ALL THE TIRES AND IS REQUESTING REIMBURSEMENT. *SLC
IN THE LAST 18 MONTHS, THREE OF THESE TIRES HAVE FAILED ON MY VAN. THE FIRST WAS A BLOWOUT THROUGH THE TREAD AREA WITH LOSS OF TREAD ESTIMATED TO BE 4" BY 8-10". THE SECOND WAS TREAD SEPARATION WITH LOSS OF A 2"BY 4" SECTION OF TREAD, THIRD TIRE HAS SUFFERED A TREAD SEPARATION APPROXIMATELY 24 INCLES LONG BY 3"-4" WIDE. I DID NOT RECORD THE DOT NUMBER INFORMATION ON THE FIRST TIRE. THE LAST TWO FAILED TIRES SHOW DOT MD11 EXOV 305. (DOT NUMBER: MD11 EXOV TIRESIZE: LT245/75R1)
THE WARRANTY WAS EXTENDED FOR THE 1994 CARS BUT NOT THE 1993 CARS. A HEAD GASKET ON A CAR SHOULD NOT BE GOING AT 73,000 MILES.
WHILE TRAVELING IN HOT WEATHER AT A LOW SPEED VEHICLE WOULD STALL WITHOUT ANY INDICATION. *AK
DD (TIRESIZE: 225/75R16M)( DOT NUMBER: TIRE SIZE: 225/75R16M )
COMPLETE TREAD SEPARATION SUDDENLY OCCURRED ON NY TURNPIKE. ALL 6 TIRES ON THIS VEHICLE WERE REPLACED WITH THIS BRAND ABOUT 10000 MILES AGO. CONCERNED ABOUT POSSIBLE FAILURE OF THE OTHER TIRES. SINCE THESE ARE NOT IN RECALL, DO I HAVE TO REPLACE ALL AT OWN EXPENSE? ANY RECOURSE FOR ME TOWARD MANUFACTURER? FAILURE CERTAINLY WAS UNUSUAL AND SCARY BUT DID NOT RESULT IN INJURY. WE HAD TO REPLACE BOTH TIRES ON REAR RIGHT BUT HAVE NOT YET REPLACED THE OTHER FOUR.REII( DOT NUMBER: TIRE SIZE: 225/75R16M )
AT APPROXIMATELY 35,000 MILES, ALL THE TIRES EXPERIENCED INTERNAL SEPERATION WHICH ALLOWED AIR PRESSURE TO PENETRATE BETWEEN THE LAYERS. THIS CAUSED BULGING WHICH WAS NOTICED BY DRIVING THE VEHICLE. WHEN THE TIRES WERE REPLACED IT WAS NOTED THAT SOME TYPE OF PATCH WAS APPLIED INTERNALLY TO THE TIRES TO "OVERCOME" THE PROBLEMS EXPERIENCED WITH THE TIRES, AS NOTED. MICHELIN SHOULD HAVE REPLACED THE TIRES AT NO CHARGE AS THEY WERE IN DANGER OF IMMINENT FAILURE! AS IT WAS, WE HAD TO PAY OVER $ 400 TO HAVE THE TIRES REPLACED. THANK YOU FOR YOUR HELP. (DOT NUMBER: NOT KNOWN TIRESIZE: LT245/75 R)
WHEN BRAKES WERE APPLIED TO DEACTIVATE THE SPEED CONTROL, VEHICLE ACCELERATED SUDDENLY AND UNEXPECTEDLY, RESULTING IN A COLLISION WHICH CAUSED MINOR INJURIES. CONSUMER HAS CONTACTED THE DEALER.*AK
NO SUMMARY LISTED FOR ABOV EVEHICLE. *AK
I RECENTLY PURCHASED THE VEHICLE AND WHEN EXAMINING THE UNDERSIDE OF THE VEHICLE I NOTICED STAINS ON FUEL LINES AND FUEL TANK FROM LEAKAGE. 1.THE FUEL RETURN HOSE IS BADLY CRACKED NEAR THE FUEL TANK AND HAS BEEN LEAKING. 2. THE FLOOR OF THE VEHICLE DIRECTLY ABOVE THE FUEL RETURN LINE IS STAINED FROM FUEL WHICH APPEARS TO HAVE BEEN SPRAYED UPWARD FROM THE FUEL LINE. 3. THERE APPEARS TO HAVE BEEN LEAKAGE ONTO THE TOP OF THE FUEL TANK WHICH HAS FLOWED DOWN THE SIDE OF THE TANK, POSSIBLY FROM THE SPRAY FROM THE FUEL RETURN LINE OR BAD GASKETS ON THE TOP OF THE FUEL TANK . 4. THERE ARE 2 DEEP CRACKS IN THE RUBBER HOSE WHICH RUNS FROM THE FUEL FILLER TO THE TANK, THERE IS NO SIGN OF LEAKAGE FROM THESE CRACKS. I FELT THAT THESE PROBLEMS SHOULD NOT BE APPEARING ON A 1993 VEHICLE AND THAT I SHOULD NOTIFY NHTSA OF THESE PROBLEMS. THANK YOU, DOUG NELSON
TIRE TREAD CAME COMPLETELY OFF TIRE. I WAS ABLE TO SAFELY STOP VEHICLE. FIRESTONE DEALER IN AURORA COLORADO, STORE # 028924 TOLD ME THAT ALL FOUR TIRES WERE MANUFACTURED AT THE DECATOR PLANT. THEY TREATED THIS LIKE A RECALL AND REPLACED ALL FOUR TIRES AT NO COST WITH GENERAL TIRES. THE FIRST TIRE TO DO EXACTLY THE SAME THING UNDER IDENTICAL CIRCUMSTANCES LOST ITS TREAD ABOUT 6 MONTHS AGO, PRIOR TO PROBLEM IDENTIFICATION AT DECATOR PLANT. SECOND TIRE CAME APART IN WYOMING. I MADE THIS REPORT THINKING THAT THE PROBLEMS AT DECATOR MIGHT EXTEND BEYOND THE TIRES CURRENTLY IDENTIFIED, AS THE AFFINITY TIRES ARE NOT ON THE RECALL LIST. THANKS. DAVE ASHTON( DOT NUMBER: TIRE SIZE: 235/75R15 )
1ST BLEWOUT ON THE HIGHWAY AT 55 MPH AND SHED THE TREAD. NO PHYSICAL DAMAGE. THE SECOND TIRE ONLY 3 WEEKS LATER HAD A DAMAGED TREAD THAT WAS NOT ROAD HAZARD. IT WAS ALSO REPLACED UNDER WARRANTY. THE 3RD TIRE HAD A BULGE ON THE SIDE WALL AND WAS REPLACED I( DOT NUMBER: TIRE SIZE: P235/75/15 )
WHILE DRIVING THE WHEEL FELL OFF THE VAN AND HIT OTHER VEHICLE ON THE ROAD (OHIO TRAFFIC CRASH REPORT). *MJS
NO SUMMARY LISTED FOR ABOVE VEHICLE. *AK
EVERY TIME THE SERPERTINE BELT TENSIONER FAIL/CRACK/BREAK THE DIESEL VEHICLE LOSES BRAKES. *AK
WHEN VAN WAS TAKEN TO THE DEALERSHIP FOR BRAKE INSPECTION, A MECHANIC FOUND A CRACKED WHEEL BEARING, WHICH COULD HAVE CAUSED THE LEFT FRONT TIRE TO COME OFF. PLEASE PROVIDE ANY FURTHER INFORMATOIN. *AK
WHEEL COULD HAVE POPPED OFF WHILE DRIVING - 2 OTHER COMPLAINTS IN NHTSA DATABASE MATCH THIS ONE. *AK
THE TRANSMISSION FAILED AT 74,000 MILES, CAUSING A REPLACEMENT, AND COST OF OVER $1,750.00. TRANSMISSION KING REPAIRED IT AND TOLD ME THAT THE FAILURE WAS DUE TO A REPAIR THAT WAS DONE BY FORD PRIOR TO ME PURCHASING IT. FORD TOLD ME IT WAS NOT A COVERED PART. *AK
LEAKING FUEL TANK DUE TO ABRASIVE WEAR AT TOP OF TANK WHERE ATTACHED TO CAR BODY.STRONG GAS FUMES FILLED THE VAN,NOTICEABLE FOR SEVERAL MONTHS, BECOMING MUCH WORSE. MECHANIC FOUND THREE HOLES INTOP OF TANK.NO BUFFERS OR PADDING WERE FOUND BETWEEN THE TANK AND BODY OF VAN.METAL AROUND HOLES BRIGHTLY WORN.SHIFTING OF GAS IN TANK FROM LEAKAGE HAD LOOSENED HOLDING STRAPS.GREAT DANGER OF FIRE.ILLNESS OF CHIEF DRIVER WITH CHEST AND LUNG PAIN FROM FUMES.
REAR BRAKE SYSTEM FAILED DUE TO CONTAMINATED (DIRTY) BRAKE FLUID.
FRONT END OUT OF ALIGNMENT. NLM
UPON FILL-UP, TOP OF TANK LEAKS LIQUID GASOLINE DOWN THE SIDES, BUT NOT AT THE FILLER NECK OR VENT NECK.
THE EXHAUST MANIFOLDS ON MY VAN FAILED ABOUT A YEAR AGO. I HAD THEM REPLACED WITH GENUINE FORD PARTS. THEY CONTINIUE TO GLOW ORANGE EVERYTIME I DRIVE THE VEHICLE. I HAVE HAD SEVERAL MECHANICS LOOK INTO THE PROBLEM WITH NO LUCK WHATSOEVER. FINALLY I CALLED MY LOCAL FORD DEALER HERE IN SANTA CRUZ, CA. NORTH BAY FORD INTIALLY AGREED THAT THE EXHAUST MANIFOLDS SHOULD NOT BE GETTING THAT HOT (GLOWING ORANGE) SO THEY RAN A BUNCH OF DIAGNOSTIC TEST(S). ALL THE ON BOARD SYTEMS CHECKED OUT AND SHOWED NO PROBLEMS SO THEY CALLED FORD HEADQUARTERS IN DEARBORN MICH. AND THE FORD TECHS SAID THAT THIS IS A NORMAL CONDITION. I DECIDED TO CALL THREE OTHER FORD DEALERSHIPS IN THE MONTEREY AND SAN JOSE AREA AND SPOKE WITH THE SERVICE PERSONS. WHEN I DESCRIBED THE PROBLEM I WAS HAVING ALL THE DEALERSHIPS RESPONDED BY ASKING ME TO MAKE AN APPOINTMENT TO HAVE THE PROBLEM FIXED. FOR THE EXAUST MANIFOLDS TO GLOW ORANGE I'M GUESSING THE ARE REACHING TEMPETURE OF NEAR 1800 DEGREES.THIS CAN'T BE NORMAL BUT IF IT IS I FEEL THAT IT MUST BE A DEFECTIVE DESIGN. PLEASE LET ME KNOW WHAT I MAY DO TO FURTHER PURSUE THIS PROBLEM. ANY HELP WOULD BE GREATLY APPRECIATED. SINCERELY, DAVID REESE (831)454-9948
THE VEHICLE STUTTERED AND WOULD MISS WHEN ACCELERATOR WAS APPLIED. DEALER SAID SOMETHING WAS WRONG WITH THE VALVE. ENGINE HAS BEEN REPLACED. *AK
TRANSMISSION OPERATES POORLY WHEN VEHICLE TEMPERATURE IS HIGH, REPLACEMENT TRANSMISSION REPEATED BEHAVIOR. MJS
ENGINE COOLANT HOSE BROKEN CAUSING LEAKAGE. MJS
UPPER AND LOWER BALL JOINT ASSEMBLY-SPINDLE ARM REPLACED, CAUSING TIRE WEAR DUE TO FAILURE. MJS
THE WIRE INSIDE THE WINDSHIELD MOTOR SHORTED OUT, CAUSING THE WINDSHIELD WIPERS TO OPERATE INTERMITTENTLY, RESULTING IN POOR VISIBILITY. *AK
3 MOUNTING BOLTS THAT HOLD FRAME OF STEERING GEAR HAVE BROKEN OFF. CAUSING LOSS OF VEHICLE CONTROL . *AK
CLUTCH ROD GOES THROUGH THE FIREWALL WHICH IS UNDER THE DASHBOARD, AND THE CLUTCH IS WORKING INTERMITTENTLY. *AK
COMPLETE ELECTRICAL SYSTEM SHUTDOWN WHEN BRAKE PEDAL IS DEPRESSED.
OIL PAN HAS CHEAP STEEL WHICH IS CAUSING CORROSION WITHIN PAN ,RESULTING IN AN OIL LEAK. *AK
POOR MATERIALS OF EXTERNAL COOLANT PIPES, WHICH RUN UNDER THE VAN, HAVE CORRODED DUE TO EXPOSURE TO WATER, ROAD SALTS,ETC. NLM
ABS VALVE WAS REMOVE AND REPLACED, DUE TO FAILURE IN BRAKE SYSTEM. *YC
THE STEERING GEAR BOX WHICH IS MOUNTED TO THE FRAME CAME OFF, CAUSING A LOSS OF STEERING WHICH COULD HAVE RESULTED IN AN ACCIDENT. *AK
NO SUMMARY
DOES NOT OPERATE : THROTTLE SOME TIMES STICKS (WHEN COLD) WHEN NOT EVEN USING CRUISE CONTROL
PLASTIC FUEL TANK SEEMS SPLIT ON TOP OF TANK.NOW LEAKING FUEL AND FUMES.TOOK IT TO FORD AND THEY SAID THEY CANNOT HELP ME BECAUSE ITS OUT OF WARRANTY.CALLED FORD'S MAIN OFFICE IN DETROIT, AND THEY ALSO SAID THEY CANNOT HELP ME. A FUEL TANK SHOULD NOT BE A PART OF A WARRANTY ITEM. THERE IS NO WEAR AND TEAR LIKE BRAKE/ENGINE/DRIVE TRAIN.ALL IT DOES IT HOLDS GASOLINE. IT SHOULD NOT CRACK OR SPLIT IN A 5 YEARS.IT SHOULD LAST ALMOST THE LIFE OF THE VEHICLE.I NOTICED THIS PROBLEM BECAUSE I CHECK UNDER MY TRUCK OFTEN. THERE COULD BE 1000'S OF VAN OUT THERE WITH THIS PROBLEM. I'M HAVING THE VAN FIXED ON THE 29TH OF JAN. 99 BY AN INDEPENDENT DEALER.HE WILL BE REPLACING THE FUEL TANK FOR APPROX. $500. I SHOULD BE REIMBURSED FOR THIS REPAIRS FROM FORD DUE TO A DEFECT OF WORKMANSHIP ON THE TANK, AND IT SHOULDN'T BE CONSIDERED A WARRANTY ITEM IN ANY VEHICLE. *AK
A LEAK HAS DEVELOPED WHERE THE GAS TANK HOSE CONNECTS TO THE FILLING /VENTING TUBE, IT APPEARS AS THOUGH WEATHER HAS CREATED THIS PROBLEM, I FEEL THAT IT IS A DESIGN FLAW BECAUSE THIS AREAIS NOT PROTECTED FROM THE ELEMENTS. POTENTIALLY VERY DANGEROUS
AS WIFE WAS TAKING OFF FROM A STOP SIGN, THE THROTTLE STUCK WIDE OPEN. DRIVER WAS ABLE TO PUT THE VAN IN NEUTRAL AND PULL OFF THE ROAD SAFELY. THE VAN WAS DRIVEN TO THE DEALERSHIP AND THE THROTTLE BODY WAS REPLACED. *AK
WHENEVER REFILLING THE GAS TANK THE GAS FUMES GET STRONGER, ALSO GAS CAME OUT OF FILLER NECK ONTO THE VEHICLE. DEALER / MFR. NOT NOTIFIED AT THIS TIME. *AK
NO SUMMARY PROVIDED BY CONSUMER
TRANSFORMER THAT IS USED TO POWER THE NEON LIGHT BEAM OVERHEATED AND CAUGHT ON FIRE. VEHICLE WAS NOT INCLUDED IN RECALL# 94V128000. CONSUMER ALSO STATES THIS PROBLEM HAS CREATED OTHER PROBLEMS WITHIN THE ELECTRICAL SYSTEM. PLEASE GIVE ANY FURTHER DETAILS. *AK
HELLO, MY NAME IS TED AND I CURRENTLY OWN 1993 FORD CLUBWAGON, AND I'VE HAD IT FOR NEARLY 5 YEARS. (PLEASE EXCUSE MY LACK OF KNOWLEDGE ABOUT THE CAR. I DON'T REALLY KNOW ABOUT PARTS OF VEHICLE.... ) ANYWAY, I'VE NEVER FOUND ANY PARTICULAR PROBLEM WITH MY CAR, EXCEPT FOR THE FACT IT TENDS TO LOSE THE WHEEL ALIGNMENT QUITE OFTEN, AND HEARD REALLY LOUD, DULL "THUMB" SOUND EVERY TIME I TURN THE STEERING WHEEL ALL THE WAY TO COUNTERCLOCKWISE. I'VE TAKEN MY VEHICLE TO FORD DEALERSHIP FOR THAT SPECIFIC PROBLEM BUT THEY COULDN'T RESOLVE THE PROBLEM. RATHER, THEY HAVE SUGGESTED AS IF IT WAS TO BE DISREGARD. FEW DAYS AGO, I PULLED MY CAR FROM THE PARKING LOT AND AGAIN, AS USUAL, I HEARD THAT "THUMP". BUT THIS TIME, THERE WAS A SMALL METALLIC PART FLEW OUT OF THE CAR. SO I BROUGHT THE CAR TO THE DEALER SERVICE CENTER AND FOUND OUT DRIVER SIDE FRONT FRAME WAS CRACKED !!!! THE CRACK RAN ALL THE WAY TO GEARBOX. AND OF COURSE, IN ORDER TO REPLACE THE FRAME COSTS FORTUNE, FOR IT WILL BE STRUCTURAL REBUILD. (THE ESTIMATE, SUM OF $6,000 OR UP, WAS MADE BY FORD DEALERSHIP). SO I CALLED THE MANUFACTURER'S CUSTOMER RELATIONS DEPARTMENT BUT UNFORTUNATELY THEY WEREN'T WILLING TO DO ANYTHING ABOUT IT. I'M SO PERPLEXED ABOUT THE FACT THAT DESPITE I HAVE MAINTAINED THE VEHICLE WELL OVER THE YEARS, THE VEHICLE IS PRACTICALLY A JUNK. TO ME, IT'S CAUSED BY MANUFACTURER'S DEFECTIVE PART, FOR THE VEHICLE WAS NEVER INVOLVED IN COLLISION. NEVER. AND AS YOU WELL KNOW, CLUBWAGON ISN'T A CARGO VAN, IT'S RATHER LUXURIOUS PASSENGER VAN. I'VE NEVER OVERLOADED THE VEHICLE WITH STUFF NOR PUT 20 PEOPLE IN IT. THEREFORE FRAME WASN'T DAMAGED DUE TO MISUSE NOR EXCEEDING ITS CAPABLE LIMIT, I BELIEVE. I'VE ONLY SEEN OR HEARD OF INCIDENTS OF BROKEN FRAME OR STRUCTURAL DAMAGE CAUSED MAJOR ACCIDENT, NOT JUST PULLING OUT OF PARKING LOT. I'M POSITIVELY CONVINCED THAT THE MANUFACTURER IS TO BLAME, AND AS I SUBMIT THE COMPLAINT, I WOULD LIKE TO TAKE AN OPPORTUNITY TO THANK YOU FOR YOUR TI.
FRONT BRAKE ROTORS WARPED CAUSING VIBRATION.
I JUST WANT TO KNOW IF THESE VANS ARE HAVING TROUBLE. THE IGNITION SWITCH SOMETIME WOULD NOT TURN OFF AND I WOULD HAVE TO WORK THE KEY AND ALSO TURN THE STEEING WHEEL BACK AND FOR TO GET THE KEY OUT. I TOOK IT TO A AUTHORIZED FORD DEALER TO HAVE REPAIRED. THEY REPLACED THE SWITCH CYLINDER THEY SAID. ONE WEEK LATER I WAS DRIVING THE VAN AND WHEN I TURNED THE WHEELS TO THE LEFT SOME TIME I WOULD HAVE TO USE FORCE TO GET THE WHEELS BACK TO THE RIGHT. THE WHEELS LOCKED UP AND I COULD NOT TURN THEM WHILE GOING TO BACK UP AND ALSO I COULD NOT GET THE TRANSMISSION OUT OF DRIVE. AGAIN THEY SAID THE CABLE TO THE TRANSMISION HAD BROKEN AND WAS REPLACED. MY QUESTION WHAT HAS TO BE DISASSEMBLED TO REPLACE THE SWITCH CYLINDER AND IF THE STEERING WHEEL HAS TO BE PULLED TO DO SO AND IF DURING REASSEMBLING THAT THE ROD THAT LOCK THE STEERING WHEEL WHEN THE IGNITION IS IN PLACE WAS DISTURBED AND HAS TO BE LINED UP. AND IF NOT PROPERLY ALINED WOULD THIS EFFECT THE STEERING OF THE VEHICLE WHEN THE KEY IS IN THE ON POSITION. I AM VERY CURIOUS DO KNOW. IF YOU COULD WOULD YOU PLEASE E-MAIL ME WITH A ANSWER. THANK YOU IN ADVANCE MILES
FUEL OVERFLOW HOSE FAILED AND LEAKES. DEALER NOTIFIED, AND WAS ABLE TO RECEIVE PART FROM PARTS SHOP. MANUFACTURER NOT NOTIFIED AT THIS TIME. *AK
CONSUMER EXPERIENCING AN ONGOING PROBLEM WITH LEAKAGE IN THE MANIFOLD. THIS CONDITION HAVE BEEN REPAIRED EVERY YEAR SINCE 1993, AND TWICE WITHIN THIS YEAR , 1998. DEALER NOTIFIED. *AK
RIM ON THE RIGHT FRONT WHEEL IS CRACKING FROM THE VALVE STEM AND CONTINUES AROUND THE RIM. THE TRUCK WAS CONVERTED BY STARCRAFT. STARCRAFT HAS BEEN NOTIFIED ABOUT THE PROBLEM. *AK
WHILE DRIVING AT 65 MPH THE TRANSMISSION DISENGAGED. OWNER HAD TO DRIVE VEHICLE IN A SECOND. VEHICLE HAS BEEN REPAIRED AT OWNER'S EXPENSE. *AK
CONSUMER COPLAINING OF GAS LEAK FROM THE HOSE BETWEEN FULLER NECK AND TANK; DEALER WILL NOT REPAIR HOSE WITHOUT COST TO THE CONSUMER. CONSUMER BELIEVES THIS PART SHOULD BE UNDER WARRANTY FOR MORE THE FIVE YEARS. *AK
CONSUMER PURCHASED COSCO MODEL # 02-086 CSS ON FEBRUARY 7, 98. CONSUMER WAS IN AN ACCIDENT AND CHILD WAS STRAPPED IN SEAT WHEN VEHICLE WENT OFF INTERSTATE AND ROLLED OVER TWICE. THE CHILD SEAT HARNESS CAME UNDONE, AND THE CHILD WAS HANGING BY HIS NECK. THE CHILD WAS CUT FROM BACK OF NECK ALL THE WAY UP.DRIVER ALSO SUFFERED INJURIES. *AK
THE CORROSION ON THE OIL PAN PROGRESSED VERY RAPIDLY, LESS THAN 5000 MILES.
POWER MIRROR SWITCH FAILED, RESULTING IN FIRE.
FRONT BRAKES JERK, VEHICLE PULLS TO RIGHT WHEN APPLIED. HAPPENS CONSTANTLY. TOOK TO DEALER 4 TIMES FOR REPAIRS & WAS UNABLE TO LOCATE PROBLEM. DEALER HAD VEHICLE UNDER WARRANTY & TECNICAL SERVICE BULLETIN. WOULD NOT REPAIR WHEN VEHICLE OUT OF WARRANTY. *AK
BOTH BOLTS ON MANIFOLD BROKE OFF, CAUSING MANIFOLD TO WARP.
DRIVER SIDE POWER MIRROR CAUSED A FIRE WHICH RESULTED IN A BURNED DOOR PANEL AND STEREO SPEAKER.
WHILE VEHICLE WAS PARKED IN DRIVEWAY WITH MOTOR RUNNING AND GEAR SHOWING PARKED, THE VAN STARTED MOVING FORWARD AND WENT THROUGH THE BACK WALL OF GARAGE. THE VAN IS CURRENTLY BEING REPAIRED. *AK
DEFECTIVE FRONT CAMBER BUSHING, CAUSING MISALIGNMENT, RESULTING IN EXCESSIVE FRONT TIRE WEAR. *AK
HYDRAULIC BRAKES: PRESSURE VALVE FAILURE. BRAKE PEDAL TRAVELS QUITE A DISTANCE BEFORE FINALLY CATCHING, CAUSING VEHICLE TO CONTINUE TRAVELING/BRAKES LOCK UP AND VEHICLE SKIDS DURING SUDDEN STOPS.
VEHICLE WAS LEFT RUNNING IN DRIVEWAY IN PARK POSITION, AND THE GEARS SHIFTED TO REVERSE AND ACCELERATED DOWN THE DRIVEWAY INTO A NEIGHBOR'S HOUSE. DEALER CAN'T FIND THE PROBLEM. *AK
TRANSMISSION FAILED.
SHOCK ABSORBERS FAILED.
THE CHECK BALL INSIDE TANK WAS CORRODED AND STUCK PREVENTING THE TANK FROM BEING FILLED.
BRAKE CALIPER PISTON DESIGN RESULTED IN BRAKE FAILURE.
WHEN DRIVING THE VEHICLE AND TRIED STOPPING THE VEHICLE AT ANY GIVEN SPEED; AND THINKING OF STEPPING ON THE BRAKE,WHEN ACTUALLY STEPPED ON THE GAS PEDAL. THE TO PEDALS ARE TOO CLOSE TOGETHER. *AK
DRIVING ABOUT 25-30MPH WHEN STEERING GEAR BOX DETACHED FROM FRAME OF VEHICLE, RESULTING IN THE LOSS OF STEERING CONTROL. TOOK TO DEALER & INFORMED DON'T KNOW WHY IT HAPPENED & WOULD TAKE A MONTH TO INVESTIGATE & FIX PROBLEM. *AK
WHEN THE TEMPERATURE REACHES 80 DEGREES OR HIGHER THERE IS A STRONG FUEL ODOR. THE HOTTER THE TEMPERATURE THE STRONGER THE ODOR. THE PROBLEM HAS NOT BEEN CORRECTED. *AK
STUDS ON LEFT REAR WHEEL BROKE, CAUSING LOSS OF WHEEL AND AN ACCIDENT. (OHIO STATE POLICE REPORT)
POWER STEERING FAILED AT LOW SPEEDS DURING WET WEATHER.
WHILE DRIVING THE VEHICLE ONE CAN HEAR THE BRAKES DRAGGING AGAINST THE ROTORS. THE ROTORS WERE REPLACED IN 4/96 WITH ABOUT 18,000 MILES ON VEHICLE BECAUSE OF WARPING. THE ROTORS HAVE BECOME WARPED AGAIN AND NEED REPLACING WITH ABOUT 28, 000 MILES. ROTORS HAVE NOT BEE REPLACED THIS TIME. *AK
WHEN APPLYING THE ABS BRAKES AT SPEEDS OF 30 TO 40MPH, THE VEHICLE SHAKES. CAUSE UNKNOWN. *AK
OWNER STATES THAT HE WAS INVOLVED IN A HEAD-ON FRONTAL ACCIDENT TRAVELING AT 35 MPH AND THERE WAS NO DEPLOYMENT OF DRIVER'S SIDE AIRBAG. OWNER IS VERY CONCERNED FOR HIS SFETY. *AK
DRIVER'S SIDE AIRBAG DIDN'T DEPLOY DURING CRASH. *AK
BALL JOINTS WEAR EXCESSIBLEY VERY QUICKLY CREATING STEERING AND VEHICLE CONTROL PROBLEMS. EXCESSIVE WEAR ON FRONT TIRE INCREASES RISK OF BLOWOUT.
FAULTY EQUALIZER VALVE, CAUSING REAR BRAKES TO BE INEFFECTIVE.
REAR ANTI-LOCK BRAKES DO NOT LOCK UP BUT MAKE THE FRONT BRAKES LOCK UP WHICH RESULTS IN LOSS OF CONTROL. *AK
WHEN THE FUEL TANK IS FILLED, A FUEL LEAK IS EXPERIENCED ON TOP OF THE TANK. THE DEALER IS UNABLE TO DETERMINE THE PROBLEM AND CAUSE. *AK
STEERING IS LOCKING CAUSING LOSS OF CONTROL.
SEAT BELT WOULD NOT RECTRACT DUE TO FAULTY RECEIVER. MJS
AIR CONDITIONER COMPRESSOR AND CLUTCH FAILED. MJS
FUEL REGULATOR ASSEMBLY FAILED. MJS
OXYGEN SENSOR FAILED. MJS
ENGINE NOISE CONTINUAL AND UNABLE TO BE RECTIFIED. MJS
THE WINDSHIELD EXHIBITS STRESS CRACKS. *AK CONSUMER STATES CRACK BEGAN AT TOP EDGE OF GLASS ABOUT 12 INCHES OF LEFT CENTER AND TO DATE HAS PROGRESED DOWNWARD AND TO A RIGHT POINT OF THE REAR VIEW MIRROR MOUNTING.*JB
FAULTY EQUALIZER VALVE CAUSED REAR BRAKE FAILURE/FRONT WHEEL LOCK.
SOMETIMES AT ANY SPEED THE VEHICLE STALLS. PLEASE DESCRIBE . *AK
FRONT UPPER BALL JOINTS FAILED. *AK
STEERING LOCKS UP WHEN BRAKES ARE APPLIED.
THE HOUSING THAT HOLDS THE LIGHT BULB MELTED . *AK ONE OF THE REAR MAP/COURTESY LIGHTS GOT STUCK IN THE ON POSITION, THIS CAUSED THE INTERIOR LIGHT HOUSING TO MELT, CONSUMER HAS THE MELTED LIGHT HOUSING. *SLC
CRUISE CONTROL STUCK AT 40 MPH.
WHEN APPLYING THE BRAKES, VEHICLE BRAKES FAILED. PLEASE DESCRIBE.*AK
VEHICLE FIRE. *SD
BRAKE FAILURE. *SD
VEHICLE DRIFTS FROM SIDE TO SIDE DUE TO STEERING MISALIGNMENT. *SD
PREMATURE FAILURE OF FRONT UPPER BALL JOINT. *DH
REAR BRAKE LINE THAT RUNS ACROSS REAR AXLE WAS WORN OUT BY A BRACKET ON BACK OF AXLE, CAUSING THE LINE TO BREAK, RESULTING IN REAR BRAKE FAILURE. *AK
WENT TO VAN AFTER SHOPPING, WINDSHIELD WIPERS WERE ON AND DASH WAS SMOKING. *AK
LOST CONRTOL OF VEHICLE, RAN INTO A DITCH TOP PORTION OF STEERING BOX BROKE. DRIVERS SIDE AIRBAG DID NOT DEPLOY. *AK
W/FRONT ABS BRAKES; BRAKE PEDAL WILL FADE WHILE APPLYING AT ANY SPEED AND HAS DONE SO (3) TIMES. PLEASE DESCRIBE DETAILS. *AK
THE VEHICLES IDLER ARM THAT HOLDS THE BELTS BROKE AND THREW THE BELTS INTO THE ENGINE FAN. THE VEHICLE LOST POWER STEERING AND POWER BRAKES. PLEASE DESCRI.
FUEL PUMP; THE CONSUMER WAS DRIVING THE VEHICLE AND THE FUEL PUMP WENT, CAUSING THE VEHICLE TO STOP IN TRIFFIC. *AK
FUEL PUMP; THE CONSUMER WAS DRIVING THE VEHICLE AND THE FUEL PUMP WENT, CAUSING THE VEHICLE TO STOP IN TRIFFIC. *AK
FUEL PUMP; THE CONSUMER WAS DRIVING THE VEHICLE AND THE FUEL PUMP WENT CAUSING THE VEHICLE TO STOP IN TRIFFIC. *AK
PURCHASE TRUCK NEW THE WHOLE TIRE WITH THE RIM CAME OFF ON TWO OCCASIONS CONSUMER WAS DRIVING WHEN THIS HAPPENED . TT
ABS; FRONT BRAKES KEEP WEARING WITHIN 20,000 MILES. REPLACE 3 TIMES ALREADY. PLEASE DESCRIBE DETAILS. TT
THE VEHICLE SHUTS DOWN W/NO WARNING MAKING STEERING DIFFICULT AND REDUCED BRAKING. NUMEROUS REPAIRS NOT CHANGE CONDITION. TT
TRUCK SHUTS DOWN W/NO WARNING MAKING STEERING DIFFICULT AND REDUCED BRAKING. NUMEROUS REPAIRS NOT CHANGE CONDITION. PLEASE DESCRIBE DETAILS. TT
TRUCK SHUTS DOWN W/NO WARNING MAKING STEERING DIFFICULT AND REDUCED BRAKING. NUMEROUS REPAIRS NOT CHANGE CONDITION. PLEASE DESCRIBE DETAILS. TT
VEHICLE OCCASIONALLY SURGES WHEN PLACED IN REVERSE. *DSH
BRAKE FAILURE, COMING DOWN INCLINE BRAKES FAILED PEDAL WENT TO THE FLOOR. TT *JB
THE ROTORS ARE WARPED AND HAVE BEEN REPLACED SEVERAL TIMES. THE TRUCK SHIMMIES VIOLENTLY WHEN STOPPING. PLEASE DESCRIBE. TT
THE REAR SOFA SEAT BELT BUCKLE IS TOO LONG DEALER CAN'T SHORTEN THE SEAT BELT . TT
POWER STEERING HAS BEEN REPAIRED SEVEN TIMES AND REPLACED FOUR TIMES. TT
ABS, WHILE DRIVING WHEN APPLYING THE BRAKES VEHICLE PULLS VERY HARD TO RIGHT, CONTINUES WEAR OF FRONT DISC ROTORS AND PADS. TT
ABS, WHILE DRIVING WHEN APPLYING THE BRAKES VEHICLE PULLS VERY HARD TO RIGHT, CONTINUES WEAR OF FRONT DISC ROTORS AND PADS. TT
ABS, WHILE DRIVING WHEN APPLYING THE BRAKES VEHICLE PULLS VERY HARD TO RIGHT, CONTINUES WEAR OF FRONT DISC ROTORS AND PADS. TT
FAULTY FUEL PUMP REPLACE 5 TIMES. TT
BRAKE HOSE NOT LONG ENOUGH TO PERMIT SUSPENSION TRAVEL WHEN WHEELS ARE TURNED HARD, CAUSING BRAKE FLUID TO LEAK FROM HOSES. *SD
PASSENGER SIDEVIEW MIRROR HAS RUBBER GROMMET BEING SAME SIZE HAS EXPOSED EDGE. DOOR/MIRROR CUT OWNERS FINGER WITH (9) STITCHES. PLEASE DESCRIBE DETAILS. TT
CONSUMER WAS DRIVING AND HIT A DEER BROKE THE RADIATOR AND THE AIR BAG DIDN'T DEPLOYED. TT
CONSUMER WAS DRIVING AND HIT A DEER BROKE THE RADIATOR AND THE AIR BAG DIDN'T DEPLOYED. TT
THE FAN BELT KEEP ON BREAKING DEALER SAY IT NOT ALIGNED RIGHT. TT
THE FAN BELT KEEP ON BREAKING DEALER SAY IT NOT ALIGNED RIGHT.
INTERIOR LIGHTS BULBS ARE OVERHEATING AND MELTING THE MATERIAL AROUND THEM. TT
WHILE ATTEMPTING TO BRAKE HAD TO APPLY EXTRA PRESSURE, LOCKED UP, HAD AN ACCIDENT. TT
WHEN DRIVING ON WET/ICY GRAVEL ROADS VEHICLE WILL NOT STOP; WITH ABS REAR BRAKES, ALL BRAKING IS ON FRONT BRAKES, CAUSING FRONT BRAKES TO LOCK UP. *AK
SERPENTINE BELT CONTINUES TO BREAK. RESULTING IN A LOSS OF POWER. TT
BRAKES LOCKS UP; HAVE TO PUSH ACCELERATOR HARD TO MOVE VEHICLE; ALSO, EMERGENCY BRAKES LOCKS UP INTERMITTENTLY. TT
BRAKES LOCKS UP; HAVE TO PUSH ACCELERATOR HARD TO MOVE VEHICLE; ALSO, EMERGENCY BRAKES LOCKS UP INTERMITTENTLY. TT
BRAKES LOCKS UP; HAVE TO PUSH ACCELERATOR HARD TO MOVE VEHICLE; ALSO, EMERGENCY BRAKES LOCKS UP INTERMITTENTLY. TT
RUBBER FUEL HOSE OF WRONG MATERIAL FOR DIESEL USE, CAUSING PREMATURE DETERIORATION OF HOSE AND SPRAYING FUEL ON ENGINE. *TW
DURING BRAKE APPLICATION ROUNDED OUT OF TURN AND VEHICLE SURGED OUT OF CONTROL TWICE, ONCE RESULTING IN AN ACCIDENT. *AK
THE SERPENTINE BELT KEEPS GOING OUT AND CAUSES THE ENTIRE AMBULANCE FAILURE. PLEASE EXPLAIN. TT
AIR CONDITIONER EVAPORATOR CAUGHT FIRE. *SKD
SHOCK ABSORBER BROKE, ALLOWING THE SPRING TO COME OUT OF PLACE. TT
TWO SEATBELT ON THE SECOND ROW IN THE MIDDLE DOES NOT RETRACT, DEALER SAID THAT IS THE WAY IT IS DESIGN. TT
DEFECTIVE DESIGN OF VEHICLES STRUCTURE CAUSES VIBRATION, LUG NUTS TO SHEAR OFF. *AW
REAR HEAT EXCHANGE HEATER CLAMP WAS INSTALLED IN A LOCATION THAT CAUSES IT TO RUB ON THE EMERGENCY BRAKE CABLE WHEN ENGAGED. *AK
REPLACED LOOSE/NOISY POWER WINDOW MOTOR ASSEMBLY. *AK
DRIVER'S DOOR LOCK JAMMED.
BRAKES FAILED, EQUIPPED WITH ABS BRAKES. TT
NO DEPLOYMENT OF AIR BAG DURING AN ACCIDENT, RESULTING IN AN INJURY. *AK
EXCESSIVE VIBRATION OF DRIVER/PASSENGER'S OUTSIDE MIRRORS. *AK
Decode a 17-digit VIN to see every complaint, recall, and safety rating for one specific vehicle.